Friday, January 23, 2026

Evektor-Aerotechnik SportStar Max, N2312T, accident occurred on December 27, 2025, at Needles Airport (EED/KEED), Needles, California

  • Location: Needles, CA 
  • Accident Number: WPR26LA073 
  • Date & Time: December 27, 2025, 11:09 Local 
  • Registration: N2312T 
  • Aircraft: EVEKTOR - AEROTECHNIK A S SPORTSTAR MAX 
  • Injuries: 2 None 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202222/pdf

http://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N2312T

On December 27, 2025, about 1109 Pacific standard time, an Evektor-Aerotechnik AS Sportstar Max LSA airplane, N2312T, was substantially damaged when it was involved in an accident near Needles, California. The pilot and pilot rated passenger were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported that while operating in cruise flight about 6,500 ft mean sea level (msl) to Lake Havasu City Airport (HII), Lake Havasu City, Arizona, all flight instruments and engine parameters were within normal operating ranges. Without warning, the airplane began vibrating violently and the control sticks moved rapidly to their forward and aft limits several. The engine RPM decreased, the vibrations simultaneously subsided and after about 15 seconds the pilot regained the ability to manipulate the control stick. The passenger observed that one of the three propeller blades had departed the propeller hub, and the pilot initiated a forced landing on runway 02 at Needles Airport (EED), Needles, California.

Post-flight inspection of the engine revealed substantial damage to the upper left engine mount which separated from the firewall. The propeller hub was fracture-separated at the blade grip. The blade grip material and the four blade retention bolts were liberated from the hub.

The airplane was recovered to a secure area for further examination.

Piper PA-28-181 Pilot 100i, N505AF, incident occurred on January 21, 2026, at Scottsdale Airport (SDL/KSDL), Scottsdale, Arizona

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N505AF

- History of Flight:
On January 21, 2026, at about 1715 local time, a Piper PA-28-181 Pilot 100i, N505AF, registered to Ameriflyers of Texas Inc and being operated as American Flyers, sustained unknown damage when it was involved in an incident at Scottsdale Airport (SDL/KSDL), Scottsdale, Arizona. The pilot was not injured.

The FAA reported: "Aircraft warming up and inadvertently started to move and struck two parked vehicles." ADS-B data showed a single ping on the far northeast side of the ramp as seen in the figure.

Figure 1: Single ping by ADS-B data recorded at 1820 LT, note close location to parked vehicles.

CubCrafters Carbon Cub FX-3, N972WY, accident occurred on January 21, 2026, near Powder River, Wyoming

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N972WY

- History of Flight:
On January 21, 2026, at about 1512 local time, a privately-registered CubCrafters Carbon Cub FX-3, N972WY, sustained substantial damage when it lost control on landing near Powder River, Wyoming. The sole pilot onboard was not injured.

Cessna 560XL Citation Excel, N802TD, accident occurred on August 14, 2025, near Oakland Park, Florida

  • Location: Oakland Park, FL 
  • Accident Number: ERA25LA301 
  • Date & Time: August 14, 2025, 17:15 Local 
  • Registration: N802TD 
  • Aircraft: Cessna 560XL 
  • Injuries: 2 None 
  • Flight Conducted Under: Part 91: General aviation - Business 

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/200796/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N802TD

On August 14, 2025, about 1715 eastern daylight time, a Cessna 560XL, N802TD, was substantially damaged when it was involved in an accident near Oakland Park, Florida. The airline transport pilot and commercial pilot were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 business flight.

The pilot and the commercial pilot arrived at Fort Lauderdale Executive Airport (KFXE), Fort Lauderdale, Florida, about 1100, with the intent to fly the airplane to Orlando Executive Airport (ORL), Orlando, Florida, with an estimated departure time of 1400. The airplane was at FXE to be painted; however, shop personnel informed them upon their arrival that the airplane was not ready to be released, and their 1400 departure time would have to be pushed back. The pilot said he utilized this time to perform a quick walk around the airplane, he adjusted the seat and rudder pedals and made plans to do a final operational check once the airplane was towed to a different location on the airport to be fueled.

The pilot said that when the airplane was ready, he performed an external pre-flight check of the airplane and arranged to add 3,500 pounds of fuel. Personnel from the paint shop arrived at the airplane, and he and the commercial pilot assisted them with multiple operational checks which included engine runs, manipulation of the control column to check flight control positioning, and cycling of the flaps from 0 to 35 degrees (five cycles). During this time, the pilot noticed that the control column seemed a bit closer than he remembered when it was full forward as compared to a different airplane of the same make and model. Otherwise, the controls seemed to move as normal with no unusual binding or limitations.

The pilot said that he and the commercial pilot completed normal pre-engine start checks, started the engines and taxied to the active runway, held short, then taxied onto the runway after receiving takeoff clearance. After taxiing onto the runway, the pilot gave the controls to the commercial pilot. The pilot said the takeoff roll was uneventful but once he retracted the landing gear, he noticed that the airplane was at an unusually high pitch and requested that the  ommercial pilot to lower the nose. He said, it became immediately obvious that she was unable to do this, so he assumed command of the airplane and placed full available forward pressure on the control column. An emergency was declared and a 180° left turn was made in an attempt to return, but both pilots were unable to arrest the climb, climbing to 9,500 ft, which was well above their assigned altitude of 2000 ft mean sea level. The tower controller asked them if they could see the runway and we were unable to see it due to the uncommanded steep climb. The tower controller then asked them to change to a Miami Air Route Traffic Control Center frequency, but he and the commercial pilot had both arms pressing forward on the control column in an attempt to prevent a stall.

Over the next several minutes, the crew attempted to maintain control of the airplane during a series of radical pitch up events into one or more stalls followed by an uncommaded steep pitch down event. The flight then proceeded towards Fort Lauderdale/Hollywood International Airport for landing on runway 10L, where the pilot performed a 360° turn to reduce airspeed. With the throttles at idle power and the speed brakes deployed, he was able to lose about 120 kts of airspeed in the 360° turn but was still about 30 knots above normal approach speed. The pilot continued towards the runway and when in ground effect, the airplane pitched up again uncommanded. The pilot was able to correct that condition and landed on the last 1/4 of the runway before he brought the airplane to a full stop. The pilots then taxied the airplane after receiving approval from emergency personnel.

Postaccident examination of the airplane revealed an elevator pushrod was bent with evidence of contact with an adjacent structural member.

Thursday, January 22, 2026

Beechcraft 35-33 Debonair, N864R, accident occurred on October 23, 2025, at Marion County Regional Airport (FLP/KFLP), Flippin, Arkansas

  • Location: Flippin, AR 
  • Accident Number: CEN26LA029 
  • Date & Time: October 23, 2025, 17:13 Local 
  • Registration: N864R 
  • Aircraft: Beech 35-33 
  • Injuries: 1 Serious 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/201921/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N864R

On October 23, 2025, about 1713 central daylight time, a Beech 35-33 airplane, N864R, was substantially damaged when it was involved in an accident near Flippin, Arkansas. The pilot sustained serious injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported that two days before the accident he flew the airplane from Dodge City Regional Airport (DDC), Dodge City, Kansas, to Marion County Regional Airport (FLP), Flippin, Arkansas. After landing, he refueled the airplane using the airport’s self-service fuel pump. After refueling, the airplane had about 63 gallons of fuel onboard. The pilot left the airplane tied down on the ramp under a fabric cover while he went fly fishing for a couple of days. The pilot returned two days later for an intended flight from FLP to DDC. He uncovered the airplane, completed a preflight inspection, started the engine normally, and taxied to the end of runway 4 where he completed an engine runup check that was part of his personal “CCEGSTAR” checklist (cabin, controls, computers, engine, gas, seatbelt, trim, altimeter, and runup).

The pilot reported that the engine parameters were nominal during the takeoff roll and that rotation and liftoff were achieved about 1,000 ft down the runway at 68 knots indicated airspeed. After liftoff, he established a positive rate of climb, retracted the landing gear, and reduced engine speed to 2,500 rpm. About midfield, he entered a climbing right turn before he leveled the wings about 150 ft above ground level (agl) at which time the airplane had a total loss of engine power.

After the loss of engine power, the pilot reduced airplane pitch and entered a left descending turn to land on the runway heading the opposite direction used for takeoff. The pilot stated that the airplane did not have sufficient altitude to reach the runway and it impacted the ground and an unoccupied skid-steer bucket loader that was parked on the airport property near the perimeter fence.

A postaccident review of recovered data from the airplane’s primary flight display (PFD) revealed normal engine operation until a sudden loss of fuel flow to the engine during initial climb. According to the recorded data, about 31 seconds after takeoff engine power was selected, the fuel flow decreased from 23.8 gallons per hour (gph) to 1.1 gph over a 10 second period. The fuel flow then decreased to 0.3 gph over the final 10 seconds of recorded data.

Two of the pilot’s friends witnessed the accident. One of the witnesses reported that shortly after takeoff he heard the airplane’s engine backfire and then a loss of engine power. The airplane entered a descending left turn and crashed on the airport property. The two witnesses immediately responded to the accident site. While driving to the accident site, one of the witnesses called 911 to report the accident. The other witnesses stated that upon arrival at the accident site he was concerned about the potential for a fire and began looking for a fire extinguisher and anything that resembled a fuel control (red-colored knobs, levers, switches). He recalled the pilot remained seated in the left cockpit seat and was bleeding from a chin laceration. He reached into the cockpit to reposition the pilot, but the pilot’s legs were wedged below the instrument panel near the rudder pedals. He stopped repositioning the pilot from the left seat after the pilot complained of back pain. The witness stated that he does not recall the pilot asking him to complete any airplane specific tasks. He and the other witness waited with the pilot until emergency personnel arrived onsite.

Emergency personnel reported that the airplane’s cabin roof was removed to lift the pilot from the left cockpit seat. The pilot was then transferred to an ambulance for additional medical evaluation. After the pilot was removed from the airplane, emergency personnel found the airplane’s fuel selector valve in the off position. One of the emergency personnel remarked that, while seated in the airplane’s left cockpit seat, the pilot’s leg/foot position would have prevented access to the fuel selector valve.

The airplane wreckage recovery personnel noted that the fuel selector assembly was obscured by the left cockpit seat. The left cockpit seat was subsequently repositioned to observe the fuel selector assembly and its handle which was in the off position.

When interviewed, the pilot indicated that he had flown the accident airplane at least 2,200 hours since he began flying it in 1992. He stated that he never turned the fuel selector to off following a flight. He indicated that his normal routine was to takeoff with the fuel selector in the left fuel tank position because excess fuel is returned from the engine to the left fuel tank. The pilot does not recall repositioning the fuel selector valve to off after the accident but opined that his friend who responded to the accident site might have turned the fuel selector to off.

A postaccident examination of the fuel system revealed no fuel system blockages between the fuel tanks and the engine fuel manifold valve. There were several fuel line separations consistent with impact-related damage, but residual fuel was found within the remaining intact fuel lines. There was no evidence of an existing fuel leak. The fuel selector valve was found in the off position. There were no anomalies noted with the fuel selector valve when it was tested with compressed air. The fuel strainer assembly contained residual uncontaminated fuel. The auxiliary fuel pump switch was found in the off position. The auxiliary fuel pump motor functioned when battery power was applied. The engine-driven fuel pump drive coupling was found intact. The engine-driven fuel pump shaft rotated smoothly by hand. There were no mechanical issues observed with the fuel metering device. All fuel finger screens were free of contamination. The fuel flow transducer contained residual fuel and was free of contamination. There were no obstructions observed when the fuel flow transducer and fuel manifold valve were tested with compressed air.

The airplane wreckage was retained pending additional examination and component testing.

Beechcraft K35 Bonanza, N9540R, fatal accident occurred on December 23, 2025, near Summer Lake, Oregon

  • Location: Summer Lake, OR 
  • Accident Number: WPR26FA068 
  • Date & Time: December 23, 2025, 08:41 Local 
  • Registration: N9540R 
  • Aircraft: Beech K35 
  • Injuries: 1 Fatal 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202203/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N9540R

On December 23, 2025, about 0841 Pacific standard time, a Beech K35, N9540R, was substantially damaged when it was involved in an accident near Summer Lake, Oregon. The pilot was fatally injured. The airplane was being operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

According to preliminary ADS-B flight track data, the airplane departed Susanville Municipal Airport (SVE), Susanville, California about 0730 and flew northwest. About 0752, the pilot requested visual flight rules (VFR) flight following to McNary Field (SLE), Salem, Oregon, with Seattle Air Route Traffic Control Center (ARTCC). About 0759, the airplane was at an altitude of about 10,600 mean sea level (msl) and turned toward the west-northwest, and the pilot reported to the controller that he was turning due to clouds. The controller subsequently relayed a weather report and pilot report (PIREP) for light rime icing near the accident pilot’s location. The data showed that the airplane continued on a west-northwest heading for about 9 minutes and climbed to about 12,170 ft msl, before it began a left 250° turn to the northeast. The controller subsequently relayed another PIREP to the pilot for light rime icing in the area.

ADS-B data showed that the airplane continued on a northeasterly heading, at altitudes that varied between 11,370 ft msl and 12,500 ft msl for about 19 minutes. About 0827, the airplane began a left turn to the northwest and climbed to about 12,800 ft msl. About 3 minutes later, the airplane turned right, to the north-northeast and climbed to about 13,100 ft msl. At 0833, the airplane entered a descending right turn and the pilot subsequently reported to the ARTCC controller that the engine lost power. The controller advised the pilot of the closest airport, which was about 13 miles northwest of their location. The pilot subsequently reported that he was in the clouds and that ice was accumulating on the airplane. ADS-B data showed that the airplane continued the descending right turn until the end of the flight track data. The last recorded ADS-B target was at 0841, at an altitude of 6,000 ft msl, about 2,300 ft north of the accident site. 

An Alert Notice (ALNOT) was issued at 0857 and a ground search was initiated utilizing emergency locator transmitter (ELT) and iPhone crash detection signals being received. The wreckage was located that afternoon by local law enforcement about 13 miles southwest of Summer Lake, Oregon, at an elevation of 5,682 ft msl.

Examination of the accident site revealed that the airplane impacted wooded terrain near the Fremont National Forest. The wreckage debris path was about 135 ft in length and oriented on a magnetic heading of about 245°. The first identified point of contact (FIPC) was an approximately 100 ft tall tree that had been topped, about 80 ft above ground level (AGL), 130 ft from the main wreckage. The right wingtip was located about 37 ft from the FIPC. The left stabilizer and elevator were located about 75 ft from the FIPC. The left wing was suspended in a tree about 20 ft above the ground about 110 ft from the FIPC. The main wreckage came to rest inverted, on a magnetic heading of about 238°. All major structural components of the airplane were located throughout the debris path.

The wreckage was recovered to a secure facility for further examination.

Zenair CH 601 HDS Zodiac, N680LM, accident occurred on September 1, 2025, near Connerton, Florida

  • Location: Connerton, FL 
  • Accident Number: ERA25LA327 
  • Date & Time: September 1, 2025, 16:05 Local 
  • Registration: N680LM 
  • Aircraft: MARK STROUT ZENAIR ZODIAC 601HDS 
  • Injuries: 2 Minor 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/200910/pdf

https://registry.faa.gov/aircraftinquiry/Search/NNumberResult?NNumberTxt=N680LM

On September 01, 2025 about 1605 eastern standard time, an experimental amateur-built Zenith Zodiac 601 HDS, N680LM, was substantially damaged when it was involved in an accident near Connerton, Florida. The pilot and the passenger received minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported that he planned to provide rides to four relatives, each on a separate 15- minute flight with a departure from and return to Pilot Country Airport (X05), Brooksville, Florida. In preparation for these flights, the pilot purchased 3 gallons of 89 octane automotive fuel. After he added the fuel, he estimated the airplane's total fuel to be 9.8 gallons prior to the first flight. Before the passengers arrived, the pilot performed a preflight inspection of the airplane and did not notice any abnormalities. On the first two flights, the pilot noted normal engine performance, including normal temperature and pressure readings. The first flight’s duration was 16 minutes, while the second was 12 minutes.

The pilot estimated that the total fuel onboard for the accident flight was 6 to 7 gallons. The pilot stated that the airplane’s cruise fuel consumption was 3.8 to 4.0 gallons per hour (gph), and that the 4 gallons of fuel was sufficient for the upcoming 15-minute flight. The pilot departed on the third flight at 1601. He did not notice anything abnormal during the ground roll or with the initial climb rate. About 420 ft above ground level (agl), the pilot reported “the engine suddenly stopped without any warning.” He further explained there were “no abnormal noises, vibrations or power deviations” prior to the loss of engine power.

He then adjusted the airplane’s pitch attitude for best glide speed, turned into the wind and prepared for an off-field landing. The pilot attempted to restart the engine twice but was unsuccessful, though he did note that the starter was functioning during these attempts. He then performed a forced landing in a nearby field. During the landing sequence,  he airplane nosed over and came to rest inverted. The pilot was able to self-extricate, then helped his passenger through the airplane’s shattered canopy.

A Federal Aviation Administration Inspector examined the wreckage at the scene of the accident and observed substantial damage to both wings, the fuselage and rudder of the airplane. Fuel was found in both wing tanks and the fuselage-mounted tank. The header tank was not examined.

The wreckage was recovered and retained for further examination.