Tuesday, November 18, 2025

Funk B85C Bee, N24157, fatal accident occurred on November 4, 2025, near Anderson, Indiana

  • Location: Anderson, IN 
  • Accident Number: CEN26FA034 
  • Date & Time: November 4, 2025, 12:45 Local 
  • Registration: N24157 
  • Aircraft: Funk B85C 
  • Injuries: 1 Fatal 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/201954/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N24157

On November 4, 2025, about 1245 eastern standard time, a Funk B85C airplane, N24157 was destroyed when it was involved in an accident near Anderson, Indiana. The pilot was fatally injured. The airplane was operated under the provisions of Title 14 Code of Federal Regulations Part 91 as a personal flight.

The airplane departed a private grass airfield (II26) in Wolcott, Indiana, earlier on the day of the accident and was enroute to Anderson Regional Airport (AID), Anderson, Indiana. The airplane was recently purchased, and the pilot was flying the airplane to AID for the new owner. A video was taken of the airplane departing II26 for AID. No anomalies were noted with the airplane during the takeoff or departure.

An air traffic controller at the AID tower stated that the pilot reported that he was 10 miles from AID inbound for landing. The controller told the pilot to report a 2 mile final approach for runway 12. The pilot read back the request to report a 2 mile final for runway 12. The controller did not have any further contact with the pilot. The controller stated that the pilot did not seem to be in distress during the radio communications.

A witness standing in his yard at the time of the accident said that he saw the airplane fly northbound along County Road 100 West in Anderson, Indiana. The witness reported that the airplane then turned sharply to the west and then to south before it landed in a dirt field adjacent to his property. The witness stated that he thought he heard the engine popping or backfiring during the landing sequence. According to the witness, once the airplane landed, it continued to roll in a relatively straight line until it impacted a tree in his front yard. The witness said that the engine was not running during the landing rollout, but the propeller was spinning. The witness also stated that he could see the pilot, and the pilot’s eyes were open, and both of his hands were on the yoke.

After the airplane impacted the tree, a fire ignited. The witness stated that flames were coming out of the broken windshield. The witness obtained a fire extinguisher and started to extinguish the fire. People traveling on County Road 100 West stopped their vehicles and assisted in extinguishing the fire and extracting the pilot from the airplane. When asked if there was smoke or fire coming from the airplane prior to the airplane impacting the tree, the witness said there was none.

The airplane landed on a heading of about 179°. A divot in the field consistent with the size and shape of the tailwheel, marked the area where the airplane touched down. From the initial touchdown point to the tree was a single set of tire tracks. The airplane traveled about 835 ft from where it first touched down until it impacted the tree.

The front of the airplane was crushed, and tree bark was embedded in the # 3 engine cylinder. The propeller was straight and undamaged. It did not exhibit any curling or polishing. The firewall and cabin were thermally damaged. The mixture was in the full- rich position, and the throttle was partially out. The ignition was in the “both” position. Fuel selector position prior to the accident could not be determined due to the fuel selector breaking free during the impact sequence. Fuel was dripping from the fuel line attached to the fuel selector. Postaccident, about 7 gallons of fuel was drained from the airplane’s sole fuel tank.

The elevator and ailerons moved freely when the yoke was manipulated. The rudder moved freely when the rudder pedals were depressed. The brakes on both the left and right main wheels activated when the brakes were depressed.

The wings were still attached to the fuselage; however, the ribs and spars on the inboard side of both wings were cracked. The cloth fabric on the wings was rippled and wrinkled.

The #1 and #3 engine cylinders had damaged fins consistent with damage received during the impact sequence, and the #3 cylinder was displaced aft. The engine case was cracked near the #1 and #3 cylinders consistent with impact damage. The interior of all 4 cylinders was examined with a borescope, and no anomalies were noted. Thumb compressions were obtained on all 4 cylinders. All 8 spark plugs were found to be normal when tested against the Champion Aviation Check-A-Plug chart. Both the left and right magnetos fired when tested. The oil filter screen was clear of debris and the oil dipstick read “full.” The gascolator screen was clean and free of debris, and the gascolator was full of fuel. The fuel inside the gascolator was tested for water utilizing Kolor Kut Water Finding Paste®. No water was detected. The carburetor screen was clean and free of debris, and there was fuel in the carburetor bowl.

The airplane was retained for further examination.

Cirrus SR22 GTS Turbo, N237RJ, accident occurred on November 3, 2025, near Sedona Airport (SDX/KSEZ), Sedona, Arizona

  • Location: Sedona, AZ 
  • Accident Number: WPR26LA036 
  • Date & Time: November 3, 2025, 08:30 Local 
  • Registration: N237RJ 
  • Aircraft: CIRRUS DESIGN CORP SR22 
  • Injuries: 2 None 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/201955/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N237RJ

On November 3, 2025, about 0830 mountain standard time, a Cirrus SR-22, N237RJ, sustained substantial damage when it was involved in an accident near Sedona, Arizona. The pilot and passenger were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot of the airplane reported that, during the preflight inspection, no anomalies were observed, and the fuel level was about 30 gallons per side. During the takeoff roll, everything seemed normal. Shortly after rotation, the engine experienced a partial loss of power, however, there was not enough runway remaining to abort the takeoff, and the pilot continued the takeoff sequence. During the initial climb out, the pilot noticed a decrease in airspeed along with an additional loss of engine power. He elected to return to the airport, however, realized he would not be able to make it to the runway, and deployed the Cirrus Airframe Parachute System (CAPS). Subsequently, the airplane descended under the parachute canopy onto desert terrain.

Post accident examination of the airplane revealed that forward fuselage and empennage sustained substantial damage. The wreckage was recovered to a secure location for further examination.

Just Aircraft Highlander, N622SC, accident occurred on November 2, 2025, near Delta, Colorado

  • Location: Delta, CO 
  • Accident Number: CEN26LA032 
  • Date & Time: November 2, 2025, 16:30 Local 
  • Registration: N622SC 
  • Aircraft: Just Highlander 
  • Injuries: 2 Serious 
  • Flight Conducted Under: Part 91: General aviation - Instructional

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/201947/pdf

https://registry.faa.gov/aircraftinquiry/Search/NNumberResult?NNumberTxt=N622SC

On November 2, 2025, about 1630 mountain standard time, an experimental amateur-built Just Highlander airplane, N622SC, was substantially damaged when it was involved in an accident near Delta, Colorado. The flight instructor and student pilot were seriously injured. The airplane was operated as a 14 Code of Federal Regulations Part 91 instructional flight.

According to the flight instructor, the purpose of the flight was an introduction to tailwheel operations for the student pilot, who was also the airplane owner. The flight instructor stated that after about an hour of performing maneuvers, they were planning to return to the departure airport to practice landings. While maneuvering to enter the airport traffic pattern, the flight instructor noticed some engine roughness and diverted toward Westwinds Airport (D17), Delta, Colorado. The flight instructor stated that the engine instruments indicated normal readings, however the airplane was only producing partial power. The engine roughness continued, and the propeller stopped turning but the engine continued to operate with normal indications. The flight instructor noticed fluid running along the left side of the airplane and prepared for a forced landing on rough terrain. The airplane impacted the ground and came to rest inverted against a ravine wall.

The airplane will be recovered to a secure location for future examination.

Piper PA-28-235 Cherokee 235, N9143W, accident occurred on November 10, 2025, in Castle Rock, Colorado

  • Location: Castle Rock, CO 
  • Accident Number: CEN26LA042 
  • Date & Time: November 10, 2025, 18:15 Local 
  • Registration: N9143W 
  • Aircraft: Piper PA-28-235 
  • Injuries: 1 Minor, 2 None 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/201987/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N9143W

On November 10, 2025, about 1815 mountain standard time, a Piper PA-28-235 airplane, N9143W, was substantially damaged when it was involved in an accident near Castle Rock, Colorado. The pilot and one passenger reported no injuries. A second passenger reported minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported that, while in cruise flight, he observed a slight decrease in engine speed. He immediately applied carburetor heat. However, about two minutes later, the engine lost all power. The pilot’s efforts to restore engine power were unsuccessful.

The pilot executed a forced landing to road. The left wing struck a car which resulted in substantial damage to the airplane. No one in the car was injured.

An engine examination is planned following recovery of the airplane.

Rutan Long-EZ, N8183K, accident occurred on October 21, 2025, in Long Beach, California

  • Location: Long Beach, CA 
  • Accident Number: WPR26LA030 
  • Date & Time: October 20, 2025, 16:03 Local 
  • Registration: N8183K 
  • Aircraft: Rutan Long-EZ 
  • Injuries: 2 Serious 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/201912/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N8183K

On October 20, 2025, about 1603 Pacific daylight time, an experimental amateur-built Rutan Long-EZ, N8183K, was substantially damaged when it was involved in an accident in Long Beach, California. The pilot was seriously injured, and a pedestrian on the ground was seriously injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

According to the pilot, he had flown the airplane from the Compton/Woodley Airport (CPM), Compton, California, to French Valley Airport (F70), Murrieta/Temecula, California, as part of a flight of two airplanes. About 1530, the flight of two airplanes departed F70, with an intended destination of CPM.

The pilot stated that the flight from F70 to the Corona area was normal and the engine was running smoothly. As he made a turn to the west to follow highway 91, he saw the fuel flow had dropped from 7 gallons per hour to 5 gallons per hour. The engine was still running normally but he radioed the lead airplane regarding the unusual fuel flow. The pilot stated that before reaching Fullerton, fuel flow had dropped to 3 gallons per hour, but the engine continued to run smoothly. The flight of two airplanes continued toward CPM and a few seconds later, the engine “throttled back.” He switched the fuel tank, turned on the electric boost pump, and enriched the mixture. The engine surged and decreased to idle, followed by a total loss of engine power.

The pilot attempted several times to restart the engine and diverted to Long Beach Airport/Daughtery Field (LGB), Long Beach, California. The pilot configured the airplane for best glide airspeed and noted it was descending about 700 ft per minute. When he realized that he would be able to make it to LGB, he initiated a forced landing to a nearby park. He stated that as he approached the park, he did not see anyone in the flight path of the airplane.

During the forced landing to the park, the airplane struck a pedestrian. The airplane sustained substantial damage to the fuselage and both wings.

The airplane was recovered to a secure location for further examination. 

Flight Design CTSW, N531CT, accident occurred on October 17, 2025, near Casa Grande Municipal Airport (CGZ/KCGZ), Casa Grande, Arizona

  • Location: Casa Grande, AZ 
  • Accident Number: WPR26LA022 
  • Date & Time: October 17, 2025, 13:20 Local 
  • Registration: N531CT 
  • Aircraft: Flight Design GMBH CTSW 
  • Injuries: 1 Minor 
  • Flight Conducted Under: Part 91: General aviation - Personal 

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/201895/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N531CT

On October 17, 2025, about 13:20 mountain standard time, a Flight Design GMBH CTSW, N531CT, was substantially damaged when it was involved in an accident near Casa Grande, Arizona. The pilot received minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91personal flight.

The pilot reported that he sumped the fuel and found no water or contaminants, then verified 12 gallons of fuel on board by viewing the fuel sight tubes at the root of the overhead wings. The engine runup, departure and climb were uneventful. About 25 minutes into the flight the engine speed slowed unexpectedly and advancing the throttle did not change the engine speed. About 15 seconds later the engine lost total power. The pilot attempted three restarts. During the first restart, the engine started and ran normally for about 5 to 10 seconds then lost total power. During the second restart, the engine ran with partial power for about 5 to 10 seconds followed by a total loss of power. The engine did not start on the third attempt. The pilot maneuvered toward the destination airport and transmitted a mayday call over the radio. The pilot realized that there was insufficient altitude to reach the airport and performed an offairport landing on desert scrub. Upon touchdown the airplane nosed-over which substantially damaged the fuselage and rudder assembly. The pilot exited the airplane unassisted.

The airplane was recovered to a secure facility for further examination.

Cirrus SR22 G2, N972JB, incident occurred on November 14, 2025, at Robert Sibley Airport (SZY/KSZY), Selmer, Tennessee

This is preliminary information, subject to change, and may contain errors. Any errors in this post will be corrected when the preliminary report is released.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N972JB

- History of Flight:
On November 14, 2025, a privately-registered Cirrus SR22 G2, N972JB, sustained unknown damage when it was involved in an incident at Robert Sibley Airport (SZY/KSZY), Selmer, Tennessee. The pilot and passenger were not injured.

The FAA reported that the airplane experienced a brake failure while taxiing for departure veering off runway and down an embankment.

Dassault Falcon 2000, and Gulfstream G650, N829AR, incident occurred on November 15, 2025, at Athens/Ben Epps Airport (AHN/KAHN), Athens, Georgia

This is preliminary information, subject to change, and may contain errors. Any errors in this post will be corrected when the preliminary report is released.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N796RM

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N829AR

- History of Flight:
On November 15, 2025, at about 2137 local time, an unknown Dassault Falcon 2000 jet,
 was taxiing for departure when it struck a parked Gulfstream G650, N829AR, at Athens/Ben Epps Airport (AHN/KAHN), Athens, Georgia. There were no reported injuries.

The airport was at near full capacity due to a weekend game between the Georgia football team against Texas.

Update November 22: It appears that Hawker 4000 N796RM was not the one involved in this event.

Boeing 747-481 BDSF, TC-ACF, fatal accident occurred on October 20, 2025, at Hong Kong-Chek Lap Kok International Airport (HKG/VHHH)

The preliminary report for this accident was released today, I believe this is all the important parts.

https://www.tlb.gov.hk/aaia/doc/PLR-2025-04_Eng.pdf

***Synopsis***

- At approximately 03:52 hours on 20 October 2025, an ACT Airlines (Air ACT) Boeing 747-481 BDSF freighter aircraft operated on behalf of Emirates SkyCargo (flight no. UAE9788) landed on Runway 07L at Hong Kong International Airport. The co-pilot was the Pilot Flying and the captain was the Pilot Monitoring.

- After landing and when the aircraft was decelerating, an AUTOBRAKES message appeared in the Engine Indication and Crew Alerting System (EICAS) display in the cockpit. The captain took over the control of the aircraft from the co-pilot.

- The aircraft veered off to the left, resulting in a runway excursion abeam Taxiway C6.

- The aircraft subsequently collided with a stationary security ground vehicle road. The impact resulted in the ground vehicle entering the sea. sea where it came to rest.

- In the course of the runway excursion, the aircraft destroyed various airport meteorological sensor arrays, signage, the ground vehicle and a section of the perimeter fence.

- The aircraft was destroyed. The tail section separated from the aircraft during the impact sequence.

- All four crew members survived the accident. The two security staff in the ground vehicle perished.

- At the time of the accident, the weather conditions were suitable for aircraft operation. Visibility was good, which was 10 km or more. All relevant communications, navigation and surveillance and air traffic control equipment/facilities were serviceable and operating normally.

- Prior to the accident, there was no report of foreign objects on the runway, and communication between Air Traffic Control and the accident aircraft was normal.

- The Runway 07L and the associated directional signage system has been in operational use since commissioning of the New North Runway (07L/25R) in November 2022. On the day of the accident, there was no report of damage to such signage system prior to the accident.

To date, on the evidence available the AAIA has established:

The aircraft was dispatched with Minimum Equipment List 1 (MEL) items which included;

  1. A Hydraulic System 1 Reservoir cockpit indication issue resolved by maintenance staff prior to the first departure of a flight day.,
  2. Number 4 engine thrust reverser inoperative.

- After departure, the evidence available is consistent with a normal flight up to the runway excursion.

- An Autobrake 2 and Flap 25 landing was planned.
- After completing a transition to the Instrument Landing System (ILS)2 of Runway (RWY) 07L, the aircraft was cleared to land by Air Traffic Control (ATC).

- ATC also advised that the wind direction was 030 degrees 18 knots and instructed the crew that after landing to keep their speed up until vacating the runway.

- The crew read back the landing clearance indicating that they would try their best.

- After touchdown the Speed Brake Lever extended with the appropriate crew call.

- Reverse thrust of approximately 95% N1 was selected on Number 2 and Number 3 engines with Number 1 engine selected to idle reverse An AUTOBRAKES message appeared in the EICAS display.

- An AUTOBRAKES message appeared in the EICAS display.

- The Autobrake disarmed and a crew call "Manual Braking" was made.

- The captain took control of the aircraft.

Subsequently, the following data is observed from the Flight Data Recorder:

- Number 4 engine accelerated to 90% N1 forward thrust at 03:52:30 hours.

- All selected thrust reversers were stowed at 03:52:35 hours. Number 4 engine continued to accelerate to approximately 106% N1 forward thrust at 03:52:36 hours and ended up at 107% N1 at 03:52:42 hours.

- Reverse thrust of approximately 92% N1 was again selected on Number 2 engine at 03:52:41 hours. Number 1 and Number 3 engine thrust reversers were also deployed reaching reverse thrust of approximately 83% N1 and 91% N1 respectively. Those thrust reverser selections occurred after the aircraft had veered off the runway.

Examination of the flight deck showed that:

- The Autobrake selector was indicating Disarmed.

- The Speed Brake lever was in the Flight Detent position.

- Number 1, 2 and 3 engine thrust levers were closed with reverse thrust levers selected to maximum.

- The Number 4 engine thrust lever was in the full forward thrust position. Number 4 engine reverse thrust lever was fully forward.

- The Fuel Control Switches were selected to Run.

Beechcraft 95 Travel Air, N2033C, accident occurred on November 14, 2025, at Massey Ranch Airpark (X50), New Smyrna Beach, Florida

This is preliminary information, subject to change, and may contain errors. Any errors in this post will be corrected when the preliminary report is released.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N2033C

- History of Flight:
On November 14, 2025, at about 1145 local time, a Beechcraft 95 Travel Air, N2033C, registered to Pray Aviation Inc out of Augusta, Kansas, sustained substantial damage when it was involved in a gearup landing event at Massey Ranch Airpark (X50), New Smyrna Beach, Florida. The two occupants onboard were not injured.

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202021/pdf

Mooney M20C, N5651Q, incident occurred on November 13, 2025, at Hesler Airport/Noble Field (LUL/KLUL), Laurel, Mississippi

This is preliminary information, subject to change, and may contain errors. Any errors in this post will be corrected when the preliminary report is released.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N5651Q

- History of Flight:
On November 13, 2025, at about 1309 local time, a Mooney M20C, N5651Q, registered to Kingdom Air LLC, sustained unknown damage when it landed gear-up on runway 31 at Hesler Airport/Noble Field (LUL/KLUL), Laurel, Mississippi. The sole pilot onboard was not injured. The personal flight originated from Diamondhead Airport (66Y), 
Diamondhead, MS, and was destined to KLUL.

It is unknown of this was a partial gear-up or an all gear-up landing.

Piper PA-31-350 T-1020, N4112D, incident occurred on November 16, 2025, at Eek Airport (EEK/PAEE), Eek, Alaska

This is preliminary information, subject to change, and may contain errors. Any errors in this post will be corrected when the preliminary report is released.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N4112D

- History of Flight:
On November 16, 2025, at about 2030 local time, a Piper PA-31-350 T-1020, N4112D, registered to YR-Aircraft Leasing LLC out of Bethel, AK, sustained unknown damage when it suffered a nose landing gear collapse while exiting the runway at Eek Airport (EEK/PAEE), Eek, Alaska. The pilot and three passengers were not injured. The on-demand flight originated from Goodnews Airport (GNU), 
Goodnews, Alaska, and was destined to EEK.

Bell UH-1H Iroquois, N959BH, incident occurred on November 7, 2025, near Nome, Alaska

This is preliminary information, subject to change, and may contain errors. Any errors in this post will be corrected when the preliminary report is released.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N959BH

- History of Flight:
On November 7, 2025, at an unknown time, a Bell UH-1H Iroquois, N959BH, registered to and being operated by Bering Air, landed at Nome Airport and a post flight inspection revealed a dent in the tail rotor. The helicopter had just arrived following a flight from Unalakleet Airport (UNK/PAUN), Alaska. The pilot and passenger were not injured.

There were no further details given by the FAA.

Beechcraft 95-B55 Baron, N711FA, incident occurred on November 14, 2025, at Dothan Regional Airport (DHN/KDHN), Dothan, Alabama

This is preliminary information, subject to change, and may contain errors. Any errors in this post will be corrected when the preliminary report is released.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N711FA

- History of Flight:
On November 14, 2025, at about 1335 local time, a Beechcraft 95-B55 Baron, N711FA, registered to Elkhorn Valley Aviation LLC out of Fremont, Nebraska, sustained unknown damage when it was involved in a gearup landing at Dothan Regional Airport (DHN/KDHN), Dothan, Alabama. The pilot and two passengers were not injured. The cross-country flight originated from Key West International Airport (EYW/KEYW), 
Key West, Florida, and was destined to DHN.

The FAA reported that the "aircraft landed gearup," and didn't give any further details.

Piper PA-32R-301T Saratoga II TC, N327HP, accident occurred on November 16, 2025, near Williamson, Georgia

This is preliminary information, subject to change, and may contain errors. Any errors in this post will be corrected when the preliminary report is released.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N327HP

- History of Flight:
On November 16, 2025, at about 0846 local time, a Piper PA-32R-301T Saratoga II TC, N327HP, sustained substantial damage in a forced landing near Williamson, Georgia. The sole pilot onboard was not injured. The aircraft is registered to N327HP LLC out of Senoia, GA, and was being operated by the pilot on a cross-country personal flight, which originated from the Atlanta Regional Airport-Falcon Field (FFC/KFFC), Atlanta, Georgia, and was destined to an unconfirmed airport in Florida.

According to the FAA, the airplane experienced engine issues on climb out from FFC and one of the landing gear struck a powerline during the ensuing forced landing. The FAA incorrectly reported the accident location as "Concord, California."

According to preliminary ADS-B data, at 0832 LT, the airplane departed KFFC and entered a climbing left turn to an altitude of 4,900 ft. About 14 minutes into the flight, the airplane initiated a descending 180 turn and eventfully landed in the vicinity of two small GA airfields.

Figure 1: End of track