Tuesday, June 17, 2025

Zenair STOL CH 701, N514JG, fatal accident occurred on May 25, 2025, near Germack Airport (7D9), Geneva, Ohio

 

  • Location: Geneva, OH
  • Accident Number: ERA25FA211 
  • Date & Time: May 25, 2025, 10:07 Local 
  • Registration: N514JG 
  • Aircraft: Zenith STOL CH701 
  • Injuries: 1 Fatal, 1 Serious 
  • Flight Conducted Under: Part 91: General aviation - Flight test

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=514JG

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/200201/pdf

On May 25, 2025, about 1007 eastern daylight time, an experimental, amateur-built Zenith STOL CH701, N514JG, was substantially damaged when it was involved in an accident near Geneva, Ohio. The pilot was fatally injured and the pilot-rated passenger sustained serious injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 test flight.


According to the pilot-rated passenger, who was also the owner of the airplane, he purchased the airplane in October 2024. He and the pilot subsequently removed the wings and transported the airplane to Germack Airport (7D9), Geneva, Ohio. The purpose of the flight was to conduct a test flight following the airplane’s reassembly and inspection. During the preflight inspection, the pilot ensured the flight controls were free and correct and no anomalies were noted during the engine run-up check.


The passenger reported that during the initial takeoff roll, “the airplane didn’t seem like it wanted to fly”, and the takeoff was aborted. The pilot taxied the airplane back to the departure end of runway 19 and initiated a second takeoff. The airplane became airborne approximately 1,800 ft down the 3,260-ft-long paved runway. During the initial climb, at an altitude of about 150 ft above ground level (agl), the airplane was unable to gain additional altitude. The pilot then pitched the nose down to gain airspeed, but the airplane was unable to maintain level flight. A surveillance video captured the engine sound consistent with operating power as the airplane descended to the trees in a nose-up attitude (see figure 1).

The airplane impacted trees and terrain about ½ mile southwest of the departure end of the runway. The first identified point of impact was a tree about 40 ft agl. The airplane came to rest in an upright position on a heading of about 330°, and about 30 ft from the initial point of impact. Several tree limbs located within the wreckage area exhibited angular cuts with black transfer marks in their separation areas. A postcrash fire ensued and consumed majority of the fuselage and right-wing fuel tank. All major components of the airplane were accounted for within the wreckage area. Both wings were partially separated from the fuselage and exhibited semicircular impressions to their leading edges. Flight control continuity was established from the cockpit controls to the rudder and elevator. The flaperon control was observed retracted and flight control continuity was established from the cockpit to the flaperon mixer assembly and bellcranks. The left and right flaperon control rods were impact separated from the flaperons. 


About 10 gallons of fuel was recovered from the left wing. A fuel sample from the left wing was free of contaminants, and a test utilizing water-finding paste was negative for the presence of water. The fuel valve was noted in the on position and was confirmed functional during a field test using low-pressure air. Majority of the fuselage mounted fuel lines were thermally destroyed. 


The engine remained attached to the fuselage with thermal damage noted to the accessory area of the engine. The spark plug electrodes were undamaged and displayed normal wear and coloration. Both magnetos produced spark from their ignition leads during hand rotation of the attached propeller. Crankshaft continuity was established from the propeller flange to the rear gears. Valvetrain continuity was established, and compression and suction were attained from all four cylinders. No anomalies were noted to the induction air filter or exhaust system. The throttle control cable remained attached to the carburetor and was observed in the open position. The mixture control cable remained attached and was noted in the rich position. The carburetor fuel inlet screen was clear of debris. The three-bladed composite propeller remained attached to the engine. One propeller blade was separated at the hub area and the remaining two blades exhibited impact damage to their leading edges.


The wreckage was retained for further examination.

Stinson 108 Voyager, N40518 , fatal accident occurred on June 3, 2025, near near Sugar Valley Airport (5NC2), Farmington, North Carolina

  • Location: Farmington, NC 
  • Accident Number: CEN25FA194 
  • Date & Time: June 3, 2025, 11:45 Local 
  • Registration: N40158 
  • Aircraft: UNIVERSAL STINSON 108 
  • Injuries: 2 Fatal, 1 Serious 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N40158

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/200255/pdf

On June 3, 2025, about 1145 eastern daylight time, a Universal Stinson 108 airplane, N40518 was destroyed when it was involved in an accident near Farmington, North Carolina. The pilot and one passenger were fatally injured, and one passenger was seriously injured. The airplane was operated under the provisions of Title 14 Code of Federal Regulations Part 91 as a personal flight.


The airplane departed runway 2 at the Sugar Valley Airport (5NC2), Mocksville, North Carolina, and flew around the traffic pattern. Upon turning base leg for runway 2, the UNICOM operator, who was looking out the airport office window facing southeast, advised the pilot that there was a turtle on the runway. According to the UNICOM operator, the pilot landed about 1,400 ft down the 2,424 ft runway and then lifted the right main wheel to avoid the turtle. The UNICOM operator stated that she heard the pilot advance the throttle after he raised the right wheel. The airplane left her point of view, and she was unable to see the airplane after that. 


A man cutting the grass at the end of runway 2 reported that he saw the turtle on the runway and the pilot raised the right wheel to avoid the turtle. After that, the wings began to rock back and forth. Then the airplane took off again, but he lost site of the airplane when it passed behind a hangar. The airplane disappeared just over the trees on the northeast side of the runway and then he heard a loud crash and saw smoke. 


The airplane impacted a heavily forested area about 255 ft northeast of the departure end of runway 2. A post impact fire ensued. The airplane came to rest on a heading of about 100°. 


The airplane was wedged between several trees and remained in one piece except for a few pieces of fabric that were found in an adjacent stream next to the accident site. The fabric on the fuselage, cowling, and wings was completely burned off and the airplane frame was visible. The fabric on the vertical stabilizer and horizontal stabilizer was intact; however, parts of the vertical stabilizer fabric were melted. The metal rudder and elevator were not fire damaged.


The airplane came to rest on its left side with the left wing folded underneath the fuselage and the right wing bent aft. Control cable continuity was confirmed to the rudder, elevator, and right aileron. Due to impact damage, cable continuity could not be confirmed to the left aileron or flaps. 


The airplane wreckage and engine were retained for further examination.