Saturday, January 17, 2026

SilverLight American Ranger AR-1, N107AR, accident occurred on September 28, 2025, at Buckingham Field (FL59), Lehigh Acres, Florida

  • Location: Fort Myers, FL 
  • Accident Number: ERA25LA369 
  • Date & Time: September 28, 2025, 10:00 Local 
  • Registration: N107AR 
  • Aircraft: GREGORY A SPICOLA AR-1 
  • Injuries: 2 None 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/201742/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N107AR

On September 28, 2025, about 1000 EST, a Spicola AR-1 gyroplane, N107AR, was substantially damaged when it was involved in an accident at Buckingham Field Airport (FL59), Lehigh Acres, Florida. The commercial pilot and pilot-rated passenger were not injured. The gyroplane was operated as a Title 14?Code of Federal Regulations Part 91 personal flight.

The pilot stated that prior to departure he added 7 gallons of 100 low lead fuel bringing the total fuel capacity to 14 gallons. After fueling he checked the fuel tank for contaminants and there were none. He also performed a preflight inspection with no discrepancies noted. As part of his briefing to the pilot-rated passenger he informed him how to enter and exit, to keep his hands free of all controls, and do not exit the gyroplane until the main rotor blades had stopped turning. He also informed him how to put and take off the passenger restraint system including the chest strap which most aircraft do not have and therefore most pilots are not accustomed to a chest strap. Weight and balance calculations showed the gyroplane was 37 pounds below design gross weight. After engine start he taxied to the approach end of the runway where he performed an engine run-up with no discrepancies reported.

He then lined up at the end of runway 32, and with about 4,400 feet of runway available, pre rotated the main rotor to 200RPM, the higher end of the pre rotation speed due to my higher weight than solo, and released the brakes. He reported acceleration was fine and the engine RPM was 5700 and climbing, rotor speed was 250RPM and climbing. After rotation he pushed over to stay in ground effect and accelerate to the takeoff safety speed of 55 knots and started to climb at 60 knots indicated. The climb rate was good until approximately 100-150 feet above ground level, when a noticeable reduction in climb performance was observed. He ensured he had full throttle applied and visually checked that his left hand was full forward. He then checked that both electric fuel pumps were on, and there was no illumination of turbocharger caution or warning lights, the alternator lights were out, and that both magneto switches were on. He glanced at the engine RPM gauge and noticed it was reading around 5,100 RPM. It was at this time that he knew a forced landing was imminent and his primary concern was of my passenger and that he needed to maintain a proper airspeed above all else.

He pushed the nose down to maintain 55 knots and realized that the flight was no longer high enough to clear the trees at the end of the runway and was still losing altitude. He surmised that there was not enough runway and overrun available to land straight ahead. The west side of the airport had a large field but with two retention ponds running 32/14. He kept the nose down maintaining 50-55 knots and made a left turn trying to get more available landing area and to avoid the trees. At approximately 20 ft he rolled level, flared, and landed between the ponds on the upslope of the bank of the first pond, which sheared the nose landing gear. The gyroplane entered the second pond and rolled over to the right coming to rest in about 2 to 3 ft of water. He extracted himself and then moved back to help extract the passenger who had already self-extracted.

The gyroplane was recovered for further detailed examination of the engine.

Thrush S-2R-T660 Thrush 710P, N7001B, accident occurred on August 18, 2025, at Southwest Georgia Regional Airport (ABY/KABY), Albany, Georgia

  • Location: Albany, GA 
  • Accident Number: ERA25LA378 
  • Date & Time: August 18, 2025, 09:44 Local 
  • Registration: N7001B 
  • Aircraft: THRUSH AIRCRAFT LLC S2R-T660 
  • Injuries: 1 Minor 
  • Flight Conducted Under: Part 91: General aviation - Flight test

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/201791/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N7001B

On August 18, 2025, about 0944 EST, a Thrush Aircraft LLC S2R-T660, N7001B, was substantially damaged when it was involved in an accident at Southwest Georgia Regional Airport, Albany, Georgia. The commercial pilot sustained minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 special flight for the purpose of production flight test.

The pilot stated that the first two landings of the day with this airplane were uneventful, but on the third landing the left master cylinder failed while in a two-wheel landing configuration with the tail coming down. The airplane then swerved to the right at high speed. During the departure from the runway, the left tire came off of the rim which then dug into the runway surface followed by the dirt off of the runway, causing the tail of the airplane to pivot around the left main landing gear. Because of the side load force applied, the left main gear separated from the airplane during the ground loop. The propeller and left wing contacted the ground, and the airplane came to a stop. He then shut down and secured the airplane.

Three days earlier during a production flight test in the same airplane, after touchdown the left brake master cylinder failed causing the airplane to depart the runway, resulting in only damage to the left main landing gear tire. That incident was not reported to NTSB at the time and was not investigated.

Beechcraft 65-A90-1 King Air, N918MR, accident occurred on January 16, 2026, at Anchorage-Merrill Field (MRI/PAMR), Anchorage, Alaska

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N918MR

- History of Flight:
On January 16, 2026, at about 1457 local time, a Beechcraft 65-A90-1 King Air, N918MR, registered to Marc Aircraft Holding LLC out of Soldotna, AK, sustained unknown, but apparent substantial damage when it was involved in an accident at Anchorage-Merrill Field (MRI/PAMR), Anchorage, Alaska. The four occupants were not injured. The flight originated from the Soldotna Airport (SXQ/PASX), 
Soldotna, Alaska, at 1437 LT.

Preliminary information indicates the airplane landed short of runway 16, collapsing the nose gear and causing the aircraft to slide up the runway. Winds at the time were from 180° at 18 knots, gusting 33 knots.

On January 11, 2026, there was another accident at Merrill Field.

On January 20, 2026, the FAA reported: "Aircraft experienced a downdraft on final and clipped a snow bank," and rated the event as accident due to substantial damage.

- Weather:

METAR PAMR 162253Z 18019G34KT 10SM FEW023 FEW050 02/M02 A2998 RMK AO2 PK WND 20041/2159 SLP152 P0019 T00171022

METAR PAMR 162353Z 18018G33KT 10SM CLR 01/M06 A3009 RMK AO2 PK WND 19041/2331 PRESRR SLP190 60067 T00061056 10028 20006 53100

Piper PA-28R-180 Cherokee Arrow, N7661J, incident occurred on January 16, 2026, at Sacramento McClellan Airport (MCC/KMCC), Sacramento, California

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N7661J

- History of Flight:
On January 16, 2026, at about 1219 local time, a privately-registered Piper PA-28R-180 Cherokee Arrow, N7661J, sustained unknown damage when it was involved in a gearup landing at Sacramento McClellan Airport (MCC/KMCC), Sacramento, California. The sole pilot onboard was not injured. The flight originated from the Lincoln Regional Karl Harder Field (KLHM), 
Lincoln, California, at 1205.

Preliminary information indicates the pilot was conducting touch-and-go(es) at KMCC when the landing gear wouldn't retract. The pilot thel landed gearup on runway 16.

Weather:

METAR KMCC 161955Z AUTO 18005KT 7SM CLR 15/10 A3011 RMK AO2

METAR KMCC 162015Z AUTO 18005KT 7SM CLR 16/10 A3010 RMK AO2

METAR KMCC 162035Z AUTO 00000KT 8SM CLR 16/09 A3009 RMK AO2