Tuesday, May 19, 2026

Flight control sys malf/fail: Bombardier CRJ-550, N707EV, incident occurred on November 23, 2025, at Range Regional Airport (HIB/KHIB), Hibbing, Minnesota

  • Location: Hibbing, Minnesota 
  • Incident Number: ENG26LA011 
  • Date & Time: November 23, 2025, 09:50 Local 
  • Registration: N707EV 
  • Aircraft: BOMBARDIER INC CL-600-2C11 
  • Aircraft Damage: None 
  • Defining Event: Flight control sys malf/fail 
  • Injuries: 17 None 
  • Flight Conducted Under: Part 121: Air carrier - Scheduled 

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202069/pdf

https://data.ntsb.gov/Docket?ProjectID=202069

On November 23, 2025, about 0950 central standard time (CST), SkyWest Airlines flight 4229, an MHIRJ Aviation Group CL-600-2C11 (CRJ550), N707EV, experienced a restriction in nose-up pitch control during the flare while landing at Range Regional Airport (KHIB), Hibbing, Minnesota. Despite the control issue, the airplane touched down and taxied to the gate with no further issues. The flight was operated as a Title 14 Code of Federal Regulations Part 121 scheduled domestic flight from Minneapolis-Saint Paul International Airport (KMSP), St. Paul, MN to KHIB. There were no injuries to occupants and there was no damage to the aircraft. 

SkyWest Airlines maintenance found that the elevator autopilot servo control cable (part number BA670-93710-13) was broken, and that the slack in the broken cable was wrapped around the autopilot servo mount in such a way that it caused the pitch restriction. Previous events investigated by the National Transportation Safety Board (NTSB) (see NTSB Investigation Number ENG25LA009) found that when this cable fails, the slack in the broken cable bound between the elevator autopilot servo mount and the cable guide pins. The bound cable interfered with the rotation of the servo mount, which remained connected to the aft side of the elevator control quadrant by the intact aft cables. This condition resulted in the limited rotation of the elevator control quadrant in one direction. 

The broken cable was sent to the NTSB Materials Laboratory for further examination. The construction of the cable was 7x7 and made from carbon steel. The fracture occurred 14 inches from the elevator autopilot servo mount end. Examination revealed that the individual wires near the fracture were worn and exhibited features consistent with cyclic fatigue. SkyWest Airlines reported that the airplane had accrued 44,643 flight hours and 33,624 flight cycles at the time of the cable failure. The cable was last inspected per MRB Task 273000-201A in May of 2016, 11,915 flight hours prior to the failure. SkyWest Airlines stated that the cable had not been replaced since they acquired the airplane in June of 2020.

Additional Reported Cable Failures 

On January 31, 2026, SkyWest Airlines maintenance personnel found the elevator autopilot servo control cable (part number BA670-93710-13) broken on a CRJ700 (registration number N707SK). The report that prompted maintenance to troubleshoot the airplane stated that greater than normal elevator back pressure was needed to control aircraft pitch. The airplane had accrued 51,171 flight hours and 34,606 flight cycles at the time of the cable failure. The cable was last inspected per MRB Task 273000-201A in April 2025, 1,802 flight hours before the failure occurred. SkyWest Airlines stated that the cable had not been replaced since they acquired the airplane in May of 2005. The NTSB did not request the failed cable for laboratory analysis due to its similarities with the incident cable failure and the failures documented in NTSB Investigation Number ENG25LA009.

Corrective Actions 

MHIRJ released service bulletins SB 670BA-27-078 and SB 601R-27-167, both dated 01 October 2025, to provide instruction to replace the affected cables on CRJ 200/550/700/900/1000 based on accrued flight hours of the cables. Transport Canada released Airworthiness Directive number CF-2025-63 with effective date of 1 December 2025 to mandate compliance with the MHIRJ service bulletins. The Federal Aviation Administration released Airworthiness Directive number 2026-02-03 with effective date of 5 February 2026 to require replacing the elevator autopilot servo control cables on affected airplanes.

- Probable Cause: The elevator control restriction was caused by the failure of an elevator autopilot servo control cable which failed due to cyclic fatigue. The slack in the cable wrapped around the servo mount in such a way that it interfered with the rotation of the servo mount. The servo mount remained connected to the aft side of the elevator control quadrant by the intact aft cables. This condition resulted in the limited rotation of the elevator control quadrant in one direction.

Piper PA-28-181 Archer TX, N643FT, accident occurred on April 18, 2026, near Indiantown, Florida

  • Location: Indiantown, FL 
  • Accident Number: ERA26LA180 
  • Date & Time: April 18, 2026, 21:15 Local 
  • Registration: N643FT 
  • Aircraft: PIPER AIRCRAFT INC PA-28-181 
  • Injuries: 1 None 
  • Flight Conducted Under: Part 91: General aviation - Instructional
https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202852/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N643FT

On April 18, 2026, about 2115 eastern daylight time, a Piper PA-28-181, N643FT, was substantially damaged when it was involved in an accident near Indiantown, Florida. The private pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 instructional flight.

According to the pilot, the purpose of the flight was to perform a night flight to a non-towered airport, then return to the departure airport, as part of his flight training curriculum. He arrived at Melbourne Orlando International Airport (MLB), Melbourne, Florida, around 1400 to plan the flight. The flight plan was completed then reviewed by the flight school’s dispatch staff. About 1915, the pilot performed a preflight inspection of the airplane and did not observe any anomalies. Based on the electronic fuel gauges and by visual inspection of the fuel tanks, the pilot determined he had full fuel; however, he separately reported 40 gallons (the airplane’s total fuel capacity was 50 gallons). He then started the engine, taxied the airplane to the active runway and performed an engine runup. The engine runup was normal and included a check of the magnetos and carburetor heat functionality. The pilot departed from MLB at 1941 and landed at Palm Beach County Park Airport (LNA), West Palm Beach, Florida, after an uneventful flight, about 2045.

The pilot taxied back to runway 10 and departed at 2051, for the return flight to MLB. After departure, he maneuvered to the west to avoid nearby controlled airspace and then proceeded northbound. He climbed to 3,500 ft above mean sea level (msl) then performed the cruise checklist. About 25 minutes after departure, the airplane experienced a loss of engine power. The pilot reported that the engine rpm suddenly decreased from 2,600 to 800. He attempted to troubleshoot but was unable to restart the engine. The pilot stated that he thought he changed the fuel tanks after the loss of engine power, but that he “could be wrong.” He then declared “mayday” to air traffic control, secured the engine and prepared for a forced landing. The pilot initially attempted to divert to a nearby airport but determined that the airplane could not reach the airport and then prepared for an off-airport landing on a road. Shortly before landing, the pilot noticed cars driving on the road. The airplane subsequently touched down in a marsh, nosed over and came to rest inverted. The pilot exited the airplane through a window.

A postaccident examination of the airplane by an FAA inspector found substantial damage to the empennage and fuselage. The inspector “rocked” the wings of the airplane and heard liquid sloshing back and forth in both fuel tanks, but was unable to open the tanks due to the position of the airplane. First responders noted fluid leaking from both wings.

The wreckage was recovered and retained for further examination.

Marquart MA-5 Charger, N987JB, accident occurred on May 15, 2026, near Tucson International Airport (TUS/KTUS), Tucson, Arizona

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N987JB

- History of Flight:
On May 15, 2026, at about 1443 local time, a Marquart MA-5 Charger, N987JB, registered to Cassill Aircraft Leasing Inc, sustained substantial damage when it was involved in an accident near Tucson International Airport (TUS/KTUS), Tucson, Arizona. The pilot was not injured. The flight originated from Stellar Airpark (P19), Chandler, Arizona, at 1358.

The FAA reported that the airplane "experienced engine failure, landed on a road and struck a light pole."

ADS-B data shows that the airplane climbed to 3,800 ft and the flight appeared uneventful. About 33 minutes later, the groundspeed and altitude values began to fluctuate. The airplane entered a descent towards KTUS, but ended up landing short of the airport on a road.

Figure 1: Flightaware data, note fluctuations towards end of track.

Piper PA-28-140 Cherokee, N8714N, accident occurred on May 15, 2026, near Chandler, Arizona

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N8714N

- History of Flight:
On May 15, 2026, at about 2046 local time, a privately-registered Piper PA-28-140 Cherokee, N8714N, sustained substantial damage in a forced landing near Chandler, Arizona. The pilot suffered minor injuries. The personal flight originated from Ak-Chin Regional Airport (A39), Maricopa, Arizona, at 2011.

The FAA reported: "Aircraft experienced engine issues and made an emergency landing on a highway."

ADS-B data shows that the airplane departed A39 and conducted three touch-and-go(es) at the airport before proceeding north. The airplane climbed to about 2,900 ft before initiating a descent. At 2044, the airplane entered a descending right hand turn over an open field. The airplane circled over the field before coming to rest nose down.

According to ATC communications, the pilot reported a partial loss of engine power and that he didn't know where he was heading. The pilot additionally reported that "I am not going to make it," and when asked about the possibility of landing on a highway, stated that he didn't want to endanger anyone on the ground and that it was very dark. The airplane eventually landed next to a road, avoiding powerlines and vehicles on the ground.

Figure 1: ADS-B data

Figure 2: Ending of track

Piper PA-11 Cub Special, N4997M, accident occurred on May 15, 2026, near Big Lake, Alaska

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N4997M

- History of Flight:
On May 15, 2026, at about 1630 local time, a Piper PA-11 Cub Special, N4997M, registered to Niner-Niner-7-Mike LLC, sustained substantial damage when it was involved in an accident near Big Lake, Alaska. The pilot was not injured.

The FAA reported that the airplane landed on a sand bar and began taxiing when the pilot applied too much speed and flipped over.

Piper PA-30 Twin Comanche B, N8188Y, incident occurred on May 15, 2026, at Keystone Heights Airport (42J), Keystone Heights, Florida

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N8188Y

- History of Flight:
On May 15, 2026, at about 2222 local time, a Piper PA-30 Twin Comanche B, N8188Y, registered to Fly Anytime LLC, sustained unknown damage when it landed gearup on one of the runways at Keystone Heights Airport (42J), Keystone Heights, Florida. The pilot and three passengers were not injured. The flight originated from 
Chicago-Midway Airport (MDW/KMDW), Chicago, Illinois, at 1636.

ADS-B data suggests the airplane conducted two touch and go(es) (or flypasses?) at the airport before the incident.

Figure 1: ADS-B data

Van's RV-7, N519JS, incident occurred on May 15, 2026, at Athens/Ben Epps Airport (AHN/KAHN), Athens, Georgia

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N519JS

- History of Flight:
On May 15, 2026, at about 0928 local time, a privately-registered Van's RV-7, N519JS, sustained unknown damage when it experienced a right main gear issue on takeoff and veered off runway at Athens/Ben Epps Airport (AHN/KAHN), Athens, Georgia. The pilot was not injured.