Thursday, June 04, 2026

Boeing 767-424ER, N77066, accident occurred on May 3, 2026, at Newark Liberty International Airport (EWR/KEWR), Newark, New Jersey

  • Location: Newark, NJ 
  • Accident Number: DCA26FA194 
  • Date & Time: May 3, 2026, 17:50 UTC 
  • Registration: N77066 
  • Aircraft: Boeing 767-424ER 
  • Injuries: 1 Minor, 231 None 
  • Flight Conducted Under: Part 121: Air carrier - Scheduled

https://www.ntsb.gov/investigations/Documents/DCA26FA194%20Preliminary%20Report.pdf

https://www.ntsb.gov/investigations/Pages/DCA26FA194.aspx

On May 3, 2026, about 13:50 eastern daylight time (EDT), United Airlines flight 169, Boeing B767-424ER, N77066, struck a light pole on the New Jersey turnpike while on final approach to runway 29 at Newark Liberty International Airport (EWR), Newark, New Jersey. Debris from the light pole subsequently impacted a tractor-trailer traveling southbound on the New Jersey turnpike. The airplane landed and taxied to the gate without further incident. The 3 flight crew members, 8 cabin crew members and 220 passengers deplaned at the gate without any injury. The driver of the tractor-trailer sustained minor injuries. The damage to the airplane was substantial. 

The flight was operated under the provisions of Title 14 Code of Federal Regulations (CFR) Part 121 as a scheduled international passenger flight from Venice Marco Polo Airport (VCE), Venice, Italy to EWR. 

As part of the investigative process, the NTSB invited qualified parties to participate in the investigation. These included the Federal Aviation Administration (FAA), United Airlines, Air Line Pilots Association (ALPA), and the Boeing Company. 

An operations group was formed, and the accident flight crew were interviewed. The flight data recorder (FDR) and cockpit voice recorder (CVR) were shipped to NTSB headquarters for download by the Research and Engineering Recorders Lab. Both recorders were downloaded successfully and a CVR group was formed. A vehicle performance specialist reviewed data from the FDR, CVR, Automatic Dependent Surveillance – Broadcast (ADS-B), and radar, along with security video. The ground proximity warning computer was also shipped to NTSB headquarters and will be downloaded at the manufacturer at a later date. Recovered pieces of the struck light pole were collected.

Crew Experience 

The flight times for the 3 flight crew members were as follows: the captain had 2,724 hours in the B757 and B767 with 378 hours as captain. The first officer had 1,958 hours and the relief officer (for the international flight) had 853 hours in the B757 and B767. Total time with United; the captain had 16,385 hours with 5,205.5 as captain and 11,179.5 as first officer, the first office had 1,958 hours, and the relief officer had 1,075 hours. Note: the flight crew members’ flight time is their time at United and does not include their flight time before being hired at United.

History of Flight 

The flight crew was originally scheduled to depart May 1st in a Boeing 757-200 from EWR, fly to Shannon Airport (SNN) in Shannon, Ireland, and back to EWR. However, the flight crew was reassigned by crew scheduling to a different airplane and route shortly before their planned departure to SNN. They were now to depart EWR in a Boeing 767-400, fly to VCE, and return to EWR. 

The first officer was the pilot flying (PF) on the outbound leg to VCE, and the captain was the PF for the return leg to EWR with the first officer the pilot monitoring (PM). Everything on the flight from VCE was normal until the descent. The flight crew planned to land on runway 4R but was changed to runway 22L during the descent. The crew was asked to prepare for holding while the airport arrival and departure pattern was changed. However, the flight did not have to hold. 

The crew slowed to 250 knots in anticipation of holding. The runway was changed again, this time to runway 29 and the crew was assigned the RNAV W RWY 29 approach, see figure 1. The captain stated he briefed the new approach after each change and that even though they were compressed briefings, all required items were covered.

The captain stated they had no CRM [crew resource management] issues on the flight. The captain was not concerned about the approach. He stated that he expected to fly the final portion of the approach at 3 red and 1 white on the Precision Approach Path Indicator (PAPI). This was his desired sight picture for runway 29. The CVR did not capture any discussion of PAPI lights for runway 29 prior to landing.

The captain stated that he turned off the autopilot and the auto-throttles at approximately 880 ft MSL or just around AXELL. He said that he “got fast” while he turned the airplane into the headwind and pulled the power levers back to compensate. The airplane shortly returned to a stable airspeed even though the wind gusts were producing “moderate turbulence.” 

The captain stated he heard the first officer call out “airspeed slow” while on short final (inside ½ mile). He mentioned that he did not receive any windshear alerts and that he always felt that the airplane was in a safe position to land. He responded to the automated 500 ft callout with the statement “stable”. 

At 500 ft, the first officer stated, they were on speed and on profile, and the captain was maintaining his planned profile of 3 red and 1 white on the PAPI. Once again, the CVR did not capture any discussion of PAPI lights for runway 29 prior to landing. Additionally, the captain, as the PF, was looking outside the airplane, and the first officer as the PM was “more committed to being inside the airplane, looking for trends.” 

As they descended, the airspeed began to decay, and the first officer recalled that he stated, “hey you are slow,” followed moments later by, “you are still slow and a little low.” The PM then looked back outside, and at that point recalled “I thought we were low”, however they were just about to touch down, and he didn’t process the information in time to get a go-around callout verbalized. The airplane landed, taxied to the gate, and all passengers and crew deplaned normally. 

The captain stated that just before touchdown “he heard a thump”. The first officer recalled feeling a mild jolt as they neared the threshold. The relief officer stated that he heard an audible thump as they went over the airport boundary a second or two before landing. After the flight landed, the purser called the flight deck and said the aft flight attendants heard a loud bang just prior to landing.

After parking at the gate, the captain went outside to assess the airplane and found damage along the aft fuselage. 

Figures 2 and 3 show the accident flight track for the RNAV approach. Figure 4 shows airspeed, ground speed, and throttle information.

At the last Meteorological Aerodrome Report (METAR) prior to landing (16:51 UTC), the wind was at 290 degrees at 19 knots, gusting to 30 knots, visibility was 10 statute miles, and the altimeter was 29.88 inches of mercury. The Terminal Area Forecast (TAF) issued at 17:24 UTC forecasted gusts up to 30 knots. The TAF issued at 14:32 UTC forecasted gusts up to 28 knots. Figure 5 shows the wind speed and direction from the FDR. 

Postaccident inspection showed all three altimeters (the captain’s, first officer’s and the standby) were accurately set to the reported altimeter setting of 29.88 Inches of mercury. To view the captain and first officer’s altimeter settings, the APU had to be started.

Runway 29

A precision Instrument Landing System (ILS) approach is not installed on runway 29 at EWR. An RNAV approach is available. It provides vertical and lateral guidance until a published Visual Guidance Fix (VGF), at which point pilots are to fly via visual reference. 

Visual guidance lighting systems (VGLS) provide visual guidance to pilots during the approach and landing phases of flight. There are multiple VGLSs with the Precision Approach Path Indicators (PAPIs) as the current standard Visual Glide Slope Indicator (VGSI) consisting of four light boxes arranged perpendicular to the edge of a runway. It projects a pattern of red and white lights that provide visual approach information along the descent path, indicating to pilots if they are high or low. 

PAPIs are designed to reduce controlled flight into terrain (CFIT) and landing distance over and under runs by assisting the pilot in establishing a stabilized descent. The display of two red lights and two white lights indicate to pilots that they are on the desired glide path to the runway.

PAPIs are normally located on the left side of runways, however the PAPIs on runway 29 at EWR are located on the right side of the runway. Figure 6 depicts the glideslope for the accident flight (red line). The green dotted line shows the altitude for a 3-degree glide slope path when the crew would see two red/two white on the PAPI. Altiudes below the grey dashed line would result in three red/one white on the PAPI. Altitudes below the grey dotted line would result in viewing four red lights on the PAPI.

Airplane and Tractor-Trailer Examination 

On site examination of the airplane revealed three punctures to the left lower aft fuselage. The damage runs from fuselage stations 1219 to 1373 and between stringers 27L and 31L. The forward puncture was about 6” long and 1” wide, the middle puncture was about 46” long and 4” wide and the aft puncture was about 8.5” long and 1” wide. Between the damaged areas there were also dents and creases on the skin. The total size of the holes was larger than the outflow valve and the damage affected all 3 elements of the fuselage structure making the damage to the airplane substantial. The #1 tire on the left main landing gear (MLG) had evidence of slash marks. See figure 7 for pictures of airplane and tire damage.

The tractor-trailer that was struck by the light pole had damage to the windshield and the side of the trailer, see figure 8. The windshield appeared to have impact damage and there were impact marks on the forward upper left corner of the trailer, and punctures in the aluminum siding. One major puncture was on the front face of the trailer, and the second puncture was minor and on the forward left side of the trailer. There was no evidence of tire marks on either the tractor cab or trailer.

Safety Actions

After the accident, United Flight Operations issued an Ops Alert that applied to EWR arrivals specific to the RNAV vertical guidance for runway 29. It reminded pilots that the visual glideslope indicator (VGSI) was designed to provide safe obstruction clearance within 10 degrees of the runway centerline up to 4 NM. In addition, United Flight Operations issued Pilot Bulletin 26-069 revision 1 to all pilots that applied to short runway landing guidance. It mentioned that a hazard was identified through their Safety Management System (SMS) that the pilot technique of shifting the aimpoint of electronic or visual glide path indications, or “ducking under”, contributes to low approach altitudes during the visual segment into certain airports and runways. It emphasized that all approaches shall be conducted so that touchdown occurs 1500’ from the runway threshold, but not prior to 1000’ from the threshold, in accordance with their Flight Manual, Chapter 3. 

The investigation is ongoing.

Sling LSA, N83PF, accident occurred on May 25, 2026, near Kalaupapa Airport (LUP/PHLU), Molokai, Hawaii

  • Location: Makanalua, HI
  • Accident Number: ANC26LA044
  • Date & Time: May 25, 2026, 11:10 Local
  • Registration: N83PF
  • Aircraft: SLING AIRCRAFT (PTY) LTD SLING LSA
  • Injuries: 2 Minor
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/203045/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N83PF

On May 25, 2026, about 1110 Hawaii-Aleutian Standard time, a Sling Aircraft LSA, N83PF, was substantially damaged when it was involved in an accident near Kalaupapa, Hawaii Airport (LUP). The two pilots onboard sustained minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight. 

The airplane was being operated by Pacific Fight Academy, a 14 CFR part 61 flight school based at Honolulu Airport (HNL), Honolulu, Hawaii. According to the private pilot, he and his pilot-rated passenger were on a cross-country flight to the Island of Molokai to build time. They flew along the coastline of Molokai and were approaching LUP, the engine began to run rough, white smoke entered the cockpit through the air vent and the engine appeared to be losing power. The pilot shut down the engine and maneuvered the airplane to line up with the runway. He felt they would not make the runway and initiated a right turn toward a nearby bay to avoid landing on the rocky coast. The airplane contacted the water and immediately became inverted; both pilots self-extricated. 

The airplane sustained substantial damage to the right wing, fuselage, and rudder. 

The accident airplane was equipped with a 100-horsepower Rotax, 912 iS Sport series engine. 

During the National Transportation Safety Board investigator-in-charge’s follow-up examination of the engine, the No. 2 cylinder exhaust valve stem was observed to be fractured from the valve spring retainer, the valve stem had fallen into the No. 2 combustion chamber, metal fragments were present in the valve covers on all cylinders.


The engine was retained by the NTSB for further examination.

Cessna 182D Skylane, N9069X, accident occurred on May 3, 2026, near Fairfield County Airport (LHQ/KLHQ), Lancaster, Ohio

  • Location: Lancaster, OH 
  • Accident Number: ERA26LA197 
  • Date & Time: May 3, 2026, 22:41 Local 
  • Registration: N9069X 
  • Aircraft: Cessna 182 
  • Injuries: 2 Minor 
  • Flight Conducted Under: Part 91: General aviation - Personal 

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202927/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N9069X

On May 3, 2026, about 2241 eastern daylight time, a Cessna 182D, N9069X, was substantially damaged when it was involved in an accident near Lancaster, Ohio. The pilot and one passenger sustained minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight. 

The pilot reported that he planned four flights the day of the accident for the purpose of building flight time. The first flight originated at Fairfield County Airport (LHQ), Lancaster, Ohio with a destination of Warren County Airport (I68), Lebanon, Ohio. The pilot completely fueled the inboard wing fuel tanks at I68, with the addition of 39 gallons of 100LL aviation gasoline. He then departed I68 and returned to LHQ. From LHQ, the pilot flew to Eastern WV Regional Airport (MRB), Martinsburg, West Virginia. The accident flight, which was the fourth and final flight for the day, departed MRB destined for LHQ. 

About 6 miles east of the LHQ airport, about 3,000 ft mean sea level, the pilot reported a partial loss of engine power, which he described as the engine “sputtering.” The pilot attempted to make an emergency landing in a field. During the landing, the airplane struck trees and impacted terrain, which resulted in substantial damage to the wings and fuselage. A witness on the ground, near the accident site heard the airplane, and described the engine noise as a “sputtering engine at low RPM.”

The airframe and engine were retained for further examination. Additionally, a JPI Fuel Scan 450 was recovered from the wreckage and forwarded to the NTSB Vehicle Recorders Laboratory, Washington, DC for download.

Beechcraft C23 Sundowner, N18516, accident occurred on May 1, 2026, at Bangor International Airport (BGR/KBGR), Bangor, Maine

  • Location: Bangor, ME 
  • Accident Number: ERA26LA196 
  • Date & Time: May 1, 2026, 16:04 Local 
  • Registration: N18516 
  • Aircraft: Beech C23 
  • Injuries: 2 None 
  • Flight Conducted Under: Part 91: General aviation - Instructional

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202926/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N18516

On May 01, 2026, at 1604 eastern daylight time, a Beechcraft C23 airplane, N18516, was substantially damaged when it was involved in an accident near Bangor, Maine. The private pilot and flight instructor were uninjured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 instructional flight.

According to the certified flight instructor (CFI), the purpose of the flight was to provide instruction to the private pilot in preparation for his commercial certificate. The CFI reported that the private pilot completed the preflight inspection with no discrepancies noted. After engine start, there was some momentary engine roughness; however, it did not last long, and the pilots continued with the lesson. Taxi, pretakeoff checks and departure from runway 33 at Bangor International Airport (BGR), Bangor, Maine, were normal.

The CFI reported that during the initial climb, about 200 ft above ground level, the pilot’s door “popped open.” The CFI contacted air traffic control (ATC) and advised that they would need to return to land to secure the door. After returning to the airport and securing the door, they taxied back to the runway for departure. The CFI continued that, after receiving a takeoff clearance, the pilot taxied into position, applied full power, and they departed from runway 33.

About 700-800 ft above mean sea level, they made a right turn to a heading of 020° and leveled the wings. The airplane subsequently began to vibrate and run rough. They elected to return to BGR. During the return, the CFI reported that the engine roughness intensified, followed by a total loss of engine power. The CFI assumed control of the airplane, declared an emergency to ATC, and maneuvered toward the runway.

While overflying the runway, the CFI realized they were too high and added flaps and slipped the airplane in an effort to lose altitude; however, the airplane floated down the runway. After touchdown, insufficient runway remained to stop. The airplane overran the runway, entered the safety area, and impacted an embankment, which resulted in substantial damage to the right wing and fuselage.

The airplane was retained for further examination.

Ryan Navion, N8618H, accident occurred on May 1, 2026, near New Salem, Massachusetts

  • Location: New Salem, MA 
  • Accident Number: ERA26LA198 
  • Date & Time: May 1, 2026, 19:10 Local 
  • Registration: N8618H 
  • Aircraft: North American Navion 
  • Injuries: 1 Minor 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202928/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N8618H

On May 1, 2026, about 1910 eastern daylight time, a North American Navion, N8618H, was substantially damaged when it was involved in an accident near New Salem, Massachusetts. The pilot received minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

According to the pilot, he conducted a routine preflight inspection, which included flight controls, oil level, and fuel sump checks. Following his inspection, he started the aircraft and taxied to the runway run-up area. The before takeoff checks were normal with no abnormalities observed before departure.

After departure, the pilot climbed to 1,700 ft mean seal level and proceeded south toward Quabbin Reservoir. Upon reaching the reservoir, he turned north toward the airport. Shortly thereafter, while in straight and level flight, the engine lost all power. The pilot established best glide speed and attempted to restart the engine without success. Realizing he could not reach the airport, and considering the local roadway traffic, tree coverage, and powerlines, he decided, the safest option was to ditch the airplane in the reservoir.

During the approach, the airplane struck trees before touching down on the surface of the water. The airplane subsequently began to sink, and the pilot egressed through the sliding canopy. The airplane sustained substantial damage to the fuselage, empennage and wings.

The wreckage was recovered and retained for further examination. 

Bushby Mustang II, N160MT, accident occurred on May 28, 2026, at Covey Trails Airport (X09), Richmond, Texas

  • Location: Richmond, TX 
  • Accident Number: CEN26LA204 
  • Date & Time: May 28, 2026, 14:40 Local 
  • Registration: N160MT 
  • Aircraft: MUSTANG AERONAUTICS MUSTANG II 
  • Injuries: 1 Minor 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/203079/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N160MT

On May 28, 2026, about 1440 central daylight time, a Mustang Aeronautics Mustang II airplane, N160MT, sustained substantial damage when it was involved in an accident near Richmond, Texas. The pilot sustained minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

According to the pilot, he had recently purchased the experimental amateur-built airplane, and the airplane was based at the Covey Trails Airport (X09), Richmond, Texas. The airplane departed from X09 and was performing multiple touch-and-go landings to the single turf runway at the airport. While performing the multiple touch-and-go landings, the pilot reported he was utilizing the carburetor heat.

During the final touch-and-go landing, just after the takeoff, the engine sustained a partial loss of power. The engine was unable to provide sufficient power to climb, and the pilot performed a forced landing. The airplane impacted a metal fence, and it came to rest upright on a flat grass field just to the south of X09 near a residential area.

The airplane sustained substantial damage to the fuselage and to both wings. The pilot reported that during the recovery of the airplane from the accident site, he drained about 10 gallons of 100 low lead fuel from the fuselage fuel tank (the sole fuel tank that has a 25-gallon useable capacity). The airplane was recovered from the accident site, and it was transported to a secure location for future examination.

The airplane, which was built in 2007, was equipped with a Lycoming O-320-E2A reciprocating engine and a Sensenich Propeller Company 70CM6S16 two-blade fixed pitch aluminum propeller.

Wednesday, June 03, 2026

NTSB Preliminary: North American F-51D Mustang, N251CS, fatal accident occurred on May 12, 2026, at Tallulah/Vicksburg Regional Airport (TVR/KTVR), Mound, Louisiana

  • Location: Mound, LA 
  • Accident Number: CEN26FA184 
  • Date & Time: May 12, 2026, 15:19 Local 
  • Registration: N251CS 
  • Aircraft: North American F-51D 
  • Injuries: 1 Fatal 
  • Flight Conducted Under: Part 91: General aviation - Personal
https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202975/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N251CS

On May 12, 2026, at 1519 central daylight time, a North American F-51D airplane, N251CS, was destroyed when it was involved in an accident at the Vicksburg Tallulah Regional Airport (TVR), Mound, Louisiana. The pilot was fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight. 

According to witnesses, the pilot was practicing an aerobatic routine. At the conclusion of the planned maneuvers, the pilot performed an additional maneuver and the airplane impacted terrain. Witnesses reported that the engine sounded normal before they heard the sound of impact. One witness, who was in a nearby hangar, reported seeing flying debris after he heard the sound of impact. A witness captured the accident sequence on a cellular phone video. According to a witness and the video, the airplane was seen climbing while conducting a maneuver consistent with a Split-S. While inverted, the airplane entered a dive and continued toward the ground in a nose low attitude. The airplane started a bank to the right just before impacting terrain in a nose level, right-wing-low attitude. The engine is heard throughout the entire video up to the sound of impact. 

The aerobatic routine was conducted within an FAA approved aerobatic practice area along the west side of runway 18/36 within the boundaries of the aerobatic box defined as a rectangular area 6,200 ft long by 2,600 ft wide, from the surface to 3,000 ft above ground level. The aerobatic practice area was active at the time of the accident. 

The airplane impacted a drainage embankment about 450 ft west of runway 18/36. The ground scars at the initial impact site were consistent with a high speed, nose level, and rightwing-low attitude. The debris field extended about 920 ft northeast of the initial impact site and was about 200 ft at its widest point. The debris field extended across a 30 ft wide drainage ditch with about 2 to 3 ft of water. All major components of the airplane were found within the debris field.

The cockpit and majority of the fuselage were about 520 ft from the initial impact site as seen in Figure 1. A propeller blade was embedded in the ground at the initial impact site. The engine separated from the airframe and was found about 690 ft from the initial impact site. The cockpit came to rest on its right side on a 300° heading. The debris field was generally aligned on a 40° heading.

Flight control continuity was confirmed for both ailerons, the elevator, and the rudder. Cable separations were consistent with overload separation due to impact damage. The majority of the fuel system was fragmented and destroyed. Both wing tank fuel bladders were breached and contained no fuel; however, fuel blight was present along the debris path on both sides of the drainage ditch. The four propeller blades exhibited leading edge damage and S-bending consistent with the production of engine power at the time of impact. 

On site examination of the airframe and engine found no anomalies that would have precluded normal operation.

A Garmin GI275 and GTN650 capable of recording data were collected on-site. The witness video of the accident and recording devices were sent to the NTSB’s Vehicle Recorders laboratory for further investigation. 

The airplane was recovered to a secure facility.