Wednesday, May 20, 2026

Air Tractor AT-602, N602RH, accident occurred on May 1, 2026, near Bealeton, Virginia

  • Location: Bealeton, VA 
  • Accident Number: ERA26LA195 
  • Date & Time: May 1, 2026, 12:30 Local 
  • Registration: N602RH 
  • Aircraft: AIR TRACTOR INC AT-602 
  • Injuries: 1 None 
  • Flight Conducted Under: Part 137: Agricultural 

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202924/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N602RH

On May 1, 2026, at 1230 eastern daylight time, an Air Tractor AT-602, N602RH, was substantially damaged when it was involved in an accident near Bealeton, Virginia. The pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 137 agricultural flight. 

The pilot reported that he was conducting an aerial application flight over a farm field and had completed previous passes uneventfully. During his last pass, the propeller blades moved uncommanded into the feather position, which resulted in a loss of thrust. The airplane was at a low altitude, and the pilot could only maneuver to a short field to make a forced landing. Upon touchdown, the pilot intentionally ground looped the airplane to avoid overrunning the field. The airplane’s landing gear collapsed, and the fuselage was substantially damaged. The airplane’s engine continued to operate with the propeller rotating until it was shut down. 

The wreckage was retained for further examination. 

Cessna 172S Skyhawk SP, N2134M, accident occurred on May 13, 2026, at Denton Enterprise Airport (DTO/KDTO), Denton, Texas

  • Location: Denton, TX
  • Accident Number: CEN26LA187
  • Date & Time: May 13, 2026, 18:15 Local
  • Registration: N2134M
  • Aircraft: Cessna 172S
  • Injuries: 1 None
  • Flight Conducted Under: Part 91: General aviation - Personal
https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202991/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?NNumberTxt=N2134M

On May 13, 2026, about 1815 central daylight time, a Cessna 172S, N2134M, sustained substantial damage when it was involved in an accident near Denton, Texas. The pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported that during takeoff roll the airplane hit something on the runway (later determined to be a gas cap from another airplane) that caused the airplane to become airborne below normal rotation (Vr) speed. The pilot stated that he attempted to reduce airplane pitch by pushing the yoke in, but the yoke was stuck and would not move. The airplane drifted to the left which the pilot attempted to counter with aileron and rudder input. Since he was unable to lower the nose of the airplane, and he was only about 5 to 7 feet above the ground, he elected to reduce engine power and the airplane impacted the ground.

Controlled flight into terr/obj (CFIT): IAI 1125 Astra SP, N1125A, fatal accident occurred on March 10, 2024, near Ingalls Field Airport (HSP/KHSP), Hot Springs, Virginia

  • Location: Hot Springs, Virginia 
  • Accident Number: ERA24FA136 
  • Date & Time: March 10, 2024, 14:52 Local 
  • Registration: N1125A 
  • Aircraft: ISRAEL AIRCRAFT INDUSTRIES 1125 WESTWIND ASTRA 
  • Aircraft Damage: Destroyed 
  • Defining Event: Controlled flight into terr/obj (CFIT) 
  • Injuries: 5 Fatal 
  • Flight Conducted Under: Part 91: General aviation - Personal 

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/193906/pdf

https://data.ntsb.gov/Docket?ProjectID=193906

On March 10, 2024, about 1452 eastern daylight time, an Israel Aircraft Industries 1125 Westwind Astra, N1125A, was destroyed when it was involved in an accident near Hot Springs, Virginia. The airline transport pilot, commercial pilot, and three passengers were fatally injured. The airplane was operated by SkyJet Elite as a Title 14 Code of Federal Regulations (CFR) Part 91 personal flight.

Following an uneventful flight, the flight crew was descending the twin-engine business jet for landing at the destination airport, which was equipped with a 5,600-ft-long runway and located on a mountain ridge. Cockpit voice recorder (CVR) audio indicated that the pilot-in-command (PIC) was the pilot flying and the second-in-command (SIC) was the pilot monitoring. Air traffic control provided the crew with the local altimeter setting as they began their descent from cruise altitude about 24 minutes before the accident. About 12 minutes later, the crew informed the controller that they had obtained the weather information at the destination. Shortly thereafter, the controller cleared the crew direct to an intermediate fix on the intended instrument landing system (ILS) approach, instructing them to cross the fix at or above 6,100 ft mean sea level (msl). The crew acknowledged and began turning toward the final approach course. About two minutes later, the controller queried the crew about their altitude, stating that he observed the airplane at 5,900 ft msl. The crew responded that they were at the assigned altitude and continued the approach. Given that the CVR did not record the crew performing any crosscheck or verification of the altimeter settings as they descended, nor did it capture the crew conducting an approach briefing, the controller’s observation that the airplane 200 ft lower than its assigned altitude suggests that the crew did not reset the airplane’s altimeter setting during the descent.

As the crew descended toward the final approach fix, the SIC asked the PIC if he would like the airplane’s flight guidance system (FGS) set to vertical speed (VS) mode, which the PIC confirmed. In this mode, the airplane’s autopilot would maintain a specified descent rate set by the crew, and would continue to descend to the set altitude at the specified rate of descent regardless of the airplane’s position on the glideslope. As the airplane neared the final approach course, the SIC stated that FLOC was captured on both sides. This likely referenced a flight management system (FMS)-generated final approach course based on the waypoints that had been programmed into the system, rather than the localizer signal broadcast by the ILS. If the ILS frequency had been tuned and selected as the navigation source, the display should have indicated LOC, not FLOC.

About 7 miles from the runway threshold (about 3 minutes before the accident), the crew began to configure the airplane for landing. The PIC stated that he had the airport in sight, and shortly thereafter, the SIC confirmed that he also had the airport in sight. Upon crossing the final approach fix, the PIC began a descent and the SIC extended the landing gear. There was no mention of a change in autopilot mode, and it is likely that this descent was also performed in VS mode. The PIC called for the before landing checklist, which the SIC completed, concluding the checklist by reporting to the PIC that the airplane was below glideslope. About 1.5 nautical miles (nm) from the runway, the SIC reported full deflection below glideslope.

Shortly thereafter, the SIC announced that the airplane was 15 knots above reference speed. About 30 seconds before the accident, the PIC turned the autopilot off. Shortly after the automated Enhanced Ground Proximity Warning System (EGPWS) 1,000-ft annunciation, the SIC suggested a go-around; the PIC did not respond. The SIC again called for a go-around just before the EGPWS 500-ft annunciation; again, the PIC did not respond. About 3 seconds later, the airplane impacted rising terrain about 300 ft before the runway threshold.

Based on the SIC’s statement that FLOC was displayed, it is likely that the flight crew did not arm the approach on either the FMS or FGS, and as a result, the system did not automatically tune the ILS frequency or capture the glideslope. Alternatively, the flight crew could have manually tuned and verified the ILS frequency on the ILS receiver. The flight crew was likely seeing advisory lateral and vertical guidance on the flight instruments based on the waypoints and altitudes input into the FMS; however, to obtain glideslope vertical guidance, the ILS frequency would need to be tuned and selected, and approach mode would need to be armed. Additionally, given the crew’s failure to properly set the altimeter, the SIC’s programming of the autopilot in VS mode to a final altitude of 4,100 ft would have resulted in the airplane descending to a true altitude between 3,800 ft and 3,900 ft before the autopilot would attempt to maintain altitude. The airport was located at an elevation about 3,792 ft msl.

The airplane’s EGPWS was capable of producing an aural “Glideslope” alert for a deviation in excess of 1.3 dots fly up (as depicted by a glideslope needle deflection of 1.3 dots above the cockpit glideslope indicator’s centerline) if the ILS was tuned and providing deviation information to the EGPWS. The accident airplane deviated beyond 1.3 dots fly up multiple times with no glideslope aural alert heard on the CVR. The EGPWS was also capable of producing radio altitude callouts for non-precision approaches and a review of the CVR found three of these callouts were heard, at 2,500 ft, 1,000 ft, and 500 ft. Based on the lack of a “Glideslope” aural alert, it is likely that the ILS was not tuned. Therefore, the flight instruments would not have received or displayed lateral localizer or vertical glideslope deviation information and the EGPWS would not have the required inputs to provide the aural “Glideslope” alert.

A review of the data recovered from the airplane’s EGPWS unit revealed that the software was not updated in accordance with an FAA special airworthiness information bulletin (SAIB) applicable to the accident airplane, nor had the EGPWS been wired directly into the airplane’s GPS as specified in the SAIB. Had the operator completed these actions, it is likely that, based on the accident flight path, the flight crew would have received an EGPWS “too low terrain” aural alert about one mile from the end of the runway, which may have prompted the PIC to take corrective action.

The PIC obtained his type rating in the accident airplane make and model about two months before the accident. A review of his training records found that multiple instructors had listed flight management system (FMS) use as one of the pilot’s weaknesses. About six months before the accident, the PIC had been dismissed from another operator due to his lack of adherence to SOPs, poor CRM, poor checklist usage, inability to manage the FMS, and poor aircraft control.

The accident airplane operator’s stabilized approach policy required that a missed approach or go-around be initiated immediately upon an approach becoming unstable below 1,000 ft above airport elevation when in instrument meteorological conditions and below 500 ft when in visual meteorological conditions. During the approach, the PIC exceeded multiple criteria that should have resulted in a missed approach or go-around, including reference speed, glideslope deviation, and descent rate parameters.

Snow showers were reported in the area around the time of the accident; however, the crew reported the airport in sight about two minutes before the accident and the CVR recording did not subsequently indicate that they lost sight of the runway. Therefore, it is likely that they remained in visual contact with the airport throughout the final portion of the approach. The wind conditions at the time of the accident were conducive to updrafts and downdrafts. It is likely that the crew encountered these conditions during the accident approach, which may have contributed to the airplane’s deviation from stabilized approach criteria and its subsequent impact with terrain; however, the PIC had ample time to complete a go-around or missed approach if he had initiated it when the approach became unstabilized. Instead, the PIC chose to continue the approach in challenging wind conditions despite exceeding multiple stabilized approach parameters.

Finally, the operator’s policy dictated that all pilots would incorporate crew resource management (CRM) considerations and practices into all aspects of flight operations. A vital CRM practice is for either crew member to be able to call for a go-around and for the pilot flying to immediately initiate the maneuver. The SIC made multiple references to the approach being unstable and twice called for a go-around. It is possible that the accident could have been prevented if the PIC had immediately initiated a go-around when the go-around call was made by the SIC.

- Probable Cause: The PIC’s continuation of an unstabilized approach in gusting wind conditions and his failure to monitor the airplane’s altitude during the approach, which led to a descent into terrain short of the runway. Contributing was the flight crew’s failure to set the appropriate altimeter setting and failure to properly configure the avionics for the ILS approach.

Loss of visual reference: Piper PA-46-310P Malibu, N85PG, fatal accident occurred on June 30, 2024, near Trout Creek, New York

  • Location: Trout Creek, New York 
  • Accident Number: ERA24FA283 
  • Date & Time: June 30, 2024, 13:55 Local 
  • Registration: N85PG 
  • Aircraft: Piper PA46 
  • Aircraft Damage: Destroyed 
  • Defining Event: Loss of visual reference 
  • Injuries: 5 Fatal 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/194574/pdf

https://data.ntsb.gov/Docket?ProjectID=194574

On June 30, 2024, at 1355 eastern daylight time, a Piper PA-46-310P airplane, N85PG, was destroyed when it was involved in an accident near Trout Creek, New York. The private pilot and four passengers were fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot filed an instrument flight rules (IFR) flight plan from the departure airport with an estimated time en route of 2 hours 47 minutes and a cruising altitude of 12,000 ft mean sea level (msl). The flight planning application the pilot used to file the flight plan provided weather briefing information, which included a convective SIGMET active for the time and route of flight and pilot weather reports (PIREPs) for turbulence and moderate chop; however, it could not be determined whether the pilot reviewed this information.

The flight departed about 45 minutes after the pilot’s filed departure time. Flight track data and air traffic control communications showed that, about 1 minute after departing, the pilot contacted air traffic control (ATC) to obtain an IFR clearance. The controller cleared the pilot to his destination as filed, issued a climb to 10,000 ft msl, and provided a weather advisory for moderate and heavy precipitation along the route, which the pilot acknowledged. About 4 minutes later, the controller issued the pilot a climb to 12,000 ft msl, which the pilot acknowledged. 

About that time, the controller began a position relief briefing with a relieving controller, which took about 2 minutes. About 2 minutes later, the new controller queried the pilot after observing that the flight had deviated left of course. The flight track data showed that, just before the query from the controller, the airplane deviated from its southwesterly ground track and began a 45-second, right 270° turn starting at an altitude of 9,800 ft msl. While in the turn, the airplane descended to an altitude of 8,700 ft msl before climbing back to an altitude of 9,800 ft msl when the airplane rolled out on an easterly ground track. About 1 minute after the query from the controller, the pilot responded, stating he had “lost” something, followed by a similar transmission 27 seconds later. This was the last transmission heard that could be attributed to the accident airplane. The airplane continued on a wavering east track for about 40 seconds, descending back down to 8,700 ft msl before climbing to 9,025 ft msl, after which the airplane entered a tight, right, descending spiral until track data was lost.

Postaccident examination of the engine and airframe found no evidence of any malfunction or failure that would have precluded normal operation of the airplane. All fracture surface and control cable separation features were consistent with overload failure. The distribution of the wreckage was consistent with an in-flight breakup of the airplane. 

The pilot’s recency and currency flying in actual instrument meteorological conditions (IMC) could not be determined. A pilot who had previously flown with the accident pilot reported that, during their last flight together (about 8 months before the accident), the accident pilot engaged the autopilot no later than 5,000 ft above ground level (agl) and continued to use the autopilot for nearly the entire flight. He also reported that, while en route, the pilot used a tablet computer to continue monitoring the weather, including looking at the weather radar. However, based on the accident flight’s heading and altitude deviations were not consistent with the autopilot being engaged; thus, it is likely the pilot was hand-flying the airplane. 

A convective SIGMET was active for the area and time of the accident. Weather radar near the time of the accident showed areas of light to heavy or extreme values of reflectivity consistent with convective activity. The cloud bases for the area were between 4,400 ft and 8,900 ft mean sea level (msl) with cloud tops between 12,500 ft and 14,500 ft msl. Based on the available weather information, the accident airplane likely entered IMC about 3 and a half minutes before the accident. Further, the accident airplane likely would have encountered moderate to severe turbulence, based on previous pilot reports and the proximity to the convective activity. 

The reduced visibility, turbulence, flight without use of the autopilot, and distraction to regain the proper course would have been conducive to the development of spatial disorientation. The resulting ground track, rapid turning descent, and in-flight breakup were consistent with a loss of control as a result of spatial disorientation.

A review of the ATC services revealed that, although the controller who informed the pilot about moderate and heavy precipitation did not use standard phraseology and did not include an area of extreme precipitation, this did not contribute to the accident. Similarly, the relieving controller’s use of nonstandard phraseology when providing the hazardous inflight weather advisory was not contributory.

- Probable Cause: The pilot’s loss of airplane control in flight due to spatial disorientation during a climb to cruise altitude in instrument meteorological conditions and turbulence, which resulted in the in-flight breakup of the airplane. Contributing to the accident was the pilot’s continued flight into an area of known convective activity.

Powerplant sys/comp malf/fail: Cessna 172R Skyhawk, N656MA, fatal accident occurred on June 11, 2024, near Gainesville Municipal Airport (GLE/KGLE), Gainesville, Texas


  • Location: Gainesville, Texas 
  • Accident Number: CEN24FA218 
  • Date & Time: June 11, 2024, 20:45 Local 
  • Registration: N656MA Aircraft: Cessna 172 
  • Aircraft Damage: Substantial 
  • Defining Event: Powerplant sys/comp malf/fail 
  • Injuries: 1 Fatal, 1 Serious 
  • Flight Conducted Under: Part 91: General aviation - Instructional 

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/194446/pdf

https://data.ntsb.gov/Docket?ProjectID=194446

On June 11, 2024, about 2045 central daylight time, a Cessna 172R, N656MA was substantially damaged when it was involved in an accident near Gainesville, Texas. The flight instructor was fatally injured, and the student was seriously injured. The flight was operated under the provisions of Title 14 Code of Federal Regulations Part 141 as an instructional flight.

The flight instructor and student pilot departed the airport, performed several flight maneuvers, and then flew to another airport to practice takeoffs and landings. On the third takeoff, the flight instructor informed the student pilot that they were low and no longer climbing. The flight instructor attempted to add more power, but the engine quit, and the propeller windmilled. The flight instructor glided the airplane to a field, hit the ground hard, bounced, and came down harder. ADS-B data revealed they had been flying for about 1 hour before the engine lost power. 

The airplane was serviced with 32.4 gallons of fuel before the flight. Aviation fuel could be smelled at the accident site and fuel blight was present on the ground underneath the airplane. Additionally, the fuel strainer bowl contained fuel. 

Postaccident examination of the engine revealed that the engine-driven fuel pump was tightly installed to the accessory section of the engine. The hose from the fuel pump to the fuel servo had about 1 ounce of fuel in it, the line from the outlet of the fuel servo to the fuel manifold had trace amounts of fuel, and a trace amount of fuel was found within the fuel manifold. There was no fuel in any of the 4 injector fuel lines. 

The top 5 screws on the engine-driven fuel pump were loose. The manufacturer stated that before the fuel pumps are stocked or shipped from their facility, they are visually inspected, at which time torque striping is applied to at least 2 of the screws. The fuel pump on the accident airplane had a torque stripe on one of the top screws and 2 of the bottom screws. All 3 torque stripes were aligned and unbroken. 

The airplane’s engine was overhauled and a new engine-driven fuel pump was installed about 5 years before the accident. The fuel pump was not a field-serviceable unit, and a review of maintenance logbooks revealed no evidence that the fuel pump was removed or serviced once it was installed. 

Because the 3 torque stripes on the screws on the fuel pump were aligned and unbroken at the time of the accident, and the fuel pump was not serviced or removed after it was installed on the overhauled engine, the top 5 screws on fuel pump likely were loose because they were improperly torqued before leaving the fuel pump manufacturing facility. 

According to the fuel pump manufacturer, if the screws are not properly torqued, the clamping force on the top 2 diaphragms could be compromised, which could lead to the fuel pump ingesting air and not operating properly. During postaccident testing of the fuel pump, air bubbles and oil were observed along the split line of the top cap. All diaphragms were intact with no damage or debris. 

The lack of a tight seal on the engine-driven fuel pump likely introduced air into the line that led to the fuel servo, which interfered with proper fuel metering within the fuel servo. The air intrusion would have disrupted the servo’s ability to meter fuel accurately because the servo relies on consistent fuel pressure and density to regulate flow. When air was present in the line, the associated pressure drop likely resulted in insufficient fuel delivery to the fuel manifold. 

The toxicological results for the flight instructor indicated use of the medication diphenhydramine which has a potential to cause sedation and cognitive psychomotor slowing. Although the pilot may have experienced impairing effects of this medication at the time of the accident, no more specific conclusion of this impairment was drawn.

- Probable Cause: The fuel pump manufacturer’s improper torquing of screws on the engine-driven fuel pump, which resulted in a disruption in the fuel system and a loss of engine power on initial climb.

Security/criminal event: Ultramagic Z-90, N290UM, fatal "accident" occurred on May 4, 2024, in Del Mar, California

  • Location: Del Mar, California 
  • Accident Number: WPR24LA142 
  • Date & Time: May 3, 2024, 18:30 Local 
  • Registration: N290UM 
  • Aircraft: Ultramagic SA Z-90 
  • Aircraft Damage: None 
  • Defining Event: Security/criminal event 
  • Injuries: 1 Fatal, 1 None 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/194216/pdf

https://data.ntsb.gov/Docket?ProjectID=194216

The flight was reported to be a celebration of life sunset flight with one passenger. Shortly after takeoff, about 1,300 ft mean sea level, the passenger asked the pilot for privacy for ceremonial reasons, and the pilot turned his back. About 20 to 30 seconds later, the pilot felt a shift in the basket and realized that the passenger had jumped from the balloon. The pilot stated he observed the passenger descending toward the ground. A postmortem report issued by the medical examiner listed the passenger’s cause of death as multiple blunt force injuries, and the manner of death as suspected suicide.

- Probable Cause: The passenger’s intentional departure from the balloon in flight as an act of suicide.

Unknown or undetermined: Cessna T240 Corvalis TTx, N636CS, fatal accident occurred on July 13, 2025, in the Pacific Ocean off San Diego, California

  • Location: San Diego, California 
  • Accident Number: WPR25LA212 
  • Date & Time: July 13, 2025, 16:29 Local 
  • Registration: N636CS Aircraft: Cessna T240 
  • Aircraft Damage: Unknown 
  • Defining Event: Unknown or undetermined 
  • Injuries: 1 Fatal 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/200551/pdf

https://data.ntsb.gov/Docket?ProjectID=200551

A family friend reported the pilot and airplane missing. The friend stated that they drove the pilot to the departure airport, dropped him off and were meeting him at the intended destination airport. The friend became concerned when the pilot did not arrive and she began to track his location on via a commercial sourced ADS-B system. She also attempted to text him but noted that her messages were not being received by the pilot’s cell phone. 

Review of the recorded communication between the air traffic controller local controller at the destination airport and the accident pilot revealed that the controller had issued landing instructions for a straight-in approach to runway 28R, which the pilot acknowledged. The controller made repeated attempts to reestablish communication with the pilot; however, no further radio communication from the pilot was received. 

ADS-B data showed that the airplane’s flight track was consistent for an approach to landing on runway 28 at the destination airport, however, the airplane continued on a southwesterly heading for about 470 nautical miles until the ADS-B data was lost. 

An Alert Notice (ALNOT) was issued about 16 minutes after ADS-B contact had been lost and a search for the pilot and airplane commenced. Neither the pilot or airplane were located. Land and sea-based searches were suspended 2 days after the airplane went missing.

- Probable Cause: Impact with the ocean for reasons that could not be determined because the pilot and airplane were not located.