Wednesday, July 01, 2026

Monnett Sonerai II, N1406, accident occurred on June 30, 2026, near Harrison County Airport (0I8), Cynthiana, Kentucky

This is preliminary information, subject to change, and may contain errors. Any errors in this writing will be corrected when/if the NTSB preliminary report is released.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N1406

- History of Flight:
On June 30, 2026, at about 1033 local time, a privately-registered Monnett Sonerai II, N1406, was destroyed when it was involved in an accident near Harrison County Airport (0I8), Cynthiana, Kentucky. The pilot was not injured. The local flight originated at 1018.

The FAA reported: "Aircraft crashed in a field for unknown reasons and caught on fire."

The pilot reported: "losing control of the plane and trying to make a landing in the level field but did not have enough power."

ADS-B data shows that the airplane departed the airport and was flying in the pattern before doing two touch-and-goes. The accident occurred during the third touch-and-go, the airplane was observed on a climbing left turn from runway 29 into the pattern, and the last ADS-B data point showed a groundspeed of 40 knots.

During the two previous initial climbs, the groundspeed was observed at ~50 knots and higher.

Figure 1: ADS-B exchange data of all touch-and-goes ran through Google Earth, note earlier part of track removed for visual clarity

Figure 2: Touch-and-go and initial climb before accident

- Weather:

METAR K27K 301415Z AUTO VRB04KT 9SM CLR 30/26 A3014 RMK AO2 T02970258

METAR K27K 301435Z AUTO 29007KT 240V310 8SM CLR 30/26 A3014 RMK AO2 T03040261

METAR K27K 301455Z AUTO VRB05KT 9SM FEW025 SCT033 31/26 A3014 RMK AO2 T03070260 51010

Revolution Aircraft Revolt, N672BB, accident occurred on June 30, 2026, at Meadow Lake Airport (FLY/KFLY), Colorado Springs, Colorado

This is preliminary information, subject to change, and may contain errors. Any errors in this writing will be corrected when/if the NTSB preliminary report is released.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N672BB

- History of Flight:
On June 30, 2026, at about 0630 local time, an Revolution Aircraft Revolt weight-shift-control aircraft, N672BB, sustained substantial damage when it was involved in an accident at Meadow Lake Airport (FLY/KFLY), Colorado Springs, Colorado. The pilot sustained serious injuries.

The FAA reported that aircraft was on takeoff and the left wing caught the runway and flipped.

- Weather:

METAR KFLY 301215Z AUTO 01004KT 10SM CLR 14/05 A3015 RMK AO2 T01400053

METAR KFLY 301235Z AUTO 01003KT 10SM CLR 15/05 A3016 RMK AO2 T01510049

METAR KFLY 301255Z AUTO 01004KT 10SM CLR 17/04 A3016 RMK AO2 T01660038

Cessna 172M Skyhawk, N6814H, accident occurred on June 30, 2026, at Lafayette Municipal Airport (3M7), Lafayette, Tennessee

This is preliminary information, subject to change, and may contain errors. Any errors in this writing will be corrected when/if the NTSB preliminary report is released.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N6814H

- History of Flight:
On June 30, 2026, at about 1747 local time, a Cessna 172M Skyhawk, N6814H, registered to Uniform Gulf Aviation LLC, sustained substantial damage when it veered off runway during departure and struck a perimeter fence at Lafayette Municipal Airport (3M7), Lafayette, Tennessee. The pilot and one passenger were not injured, and one passenger suffered minor injuries.

- Weather:

METAR KXNX 302235Z AUTO 24003KT 10SM CLR 36/21 A3009 RMK A01

METAR KXNX 302255Z AUTO 00000KT 10SM CLR 35/20 A3008 RMK A01

Cessna 172L Skyhawk, N7697G, incident occurred on June 30, 2026, at Easterwood Field Airport (CLL/KCLL), College Station, Texas

This is preliminary information, subject to change, and may contain errors. Any errors in this writing will be corrected when/if the NTSB preliminary report is released.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N7697G

- History of Flight:
On June 30, 2026, at about 1359 local time, a Cessna 172L Skyhawk, N7697G, registered to Flight School Inc, sustained unknown, but apparent minor damage when it was involved in an incident at Easterwood Field Airport (CLL/KCLL), College Station, Texas. The student pilot was not injured. The training flight originated from David Wayne Hooks Airport (DWH/KDWH), 
Houston, Texas, at 1322.

The FAA reported: "Aircraft experienced brake failure on landing and went off the end of the runway into the grass striking a threshold light."

ADS-B data shows the airplane on final approach to runway 17. The winds were from 170°at 5 knots, gusting 14 knots. The airplane was flown back to KDWH 4 hours later.

- Weather:

METAR KCLL 301853Z 17005G14KT 10SM FEW048 32/22 A3003 RMK AO2 SLP162 T03220217

METAR KCLL 301953Z 16012G19KT 10SM SCT046 33/22 A3001 RMK AO2 SLP156 T03330222

Lancair IV-PT, N815NS, incident occurred on June 30, 2026, at Greenville Downtown Airport (GMU/KGMU), Greenville, South Carolina

This is preliminary information, subject to change, and may contain errors. Any errors in this writing will be corrected when/if the NTSB preliminary report is released.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N815NS

- History of Flight:
On June 30, 2026, at about 1303 local time, a Lancair IV-PT, N815NS, registered to N815NS LLC, sustained minor damage when it suffered a nose wheel collapse during the landing sequence on runway 1 at Greenville Downtown Airport (GMU/KGMU), Greenville, South Carolina. The pilot was not injured. The flight originated from DeKalb Peachtree Airport (PDK/KPDK), 
Atlanta, Georgia, at 1222.

- Weather:

METAR KGMU 301653Z VRB03KT 10SM FEW037 SCT080 31/22 A3018 RMK AO2 SLP206 T03110217 $

METAR KGMU 301713Z VRB06KT 10SM SCT038 32/22 A3017 RMK AO2 T03220222 $

Beechcraft A36 Bonanza, N8095F, incident occurred on June 30, 2026, at Paynesville Municipal Airport (PEX/KPEX), Paynesville, Minnesota

This is preliminary information, subject to change, and may contain errors. Any errors in this writing will be corrected when/if the NTSB preliminary report is released.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N8095F

- History of Flight:
On June 30, 2026, at about 1751 local time, a privately-registered Beechcraft A36 Bonanza, N8095F, sustained unknown damage when the nose gear detached on landing runway 29 at Paynesville Municipal Airport (PEX/KPEX), Paynesville, Minnesota. The pilot and passenger were not injured. The flight originated from Ames Municipal Airport (AMW/KAMW), 
Ames, Iowa, at 1633.

The winds were from 250° at 8 knots, gusting 14 knots.

- Weather:

METAR KPEX 302235Z AUTO 22009KT 10SM CLR 29/14 A2978 RMK AO2 TSNO

METAR KPEX 302255Z AUTO 25008G14KT 10SM CLR 29/14 A2978 RMK AO2 TSNO

Tuesday, June 30, 2026

Loss of control in flight: Cirrus SR22 GTS G6 carbon, N990PT, fatal accident occurred on July 25, 2024, at Hancock County-Bar Harbor Airport (BHB/KBHB), Trenton, Maine

  • Location: Trenton, Maine 
  • Accident Number: ERA24FA323 
  • Date & Time: July 25, 2024, 12:27 Local 
  • Registration: N990PT 
  • Aircraft: CIRRUS DESIGN CORP SR22 
  • Aircraft Damage: Destroyed 
  • Defining Event: Loss of control in flight 
  • Injuries: 2 Fatal 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/194767/pdf

https://data.ntsb.gov/Docket?ProjectID=194767 

On July 25, 2024, about 1227 eastern daylight time, a Cirrus Design Corp SR22 airplane, N990PT, was destroyed when it was involved in an accident near Trenton, Maine. The pilot and passenger were fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot received a weather briefing package from a commercial service when he filed his instrument flight rules (IFR) flight plan before departing on the accident flight. The weather briefing information the pilot received included forecasts and AIRMETs for low IFR (LIFR) conditions at the destination airport during the planned time of arrival (LIFR, refers to a cloud ceiling below 500 ft above ground level [agl] and/or visibility less than 1 mile). Reported conditions at the destination airport about 31 minutes before the accident included visibility of 1.5 miles in light rain and mist and an overcast ceiling at 300 ft agl. As the flight neared the destination airport, an air traffic controller provided the pilot with a radar vector, cleared the flight for an instrument landing system (ILS) approach. The ILS approach specified a minimum visibility of 3/4 mile and a decision height of 200 ft agl, or 283 ft mean seal level (msl).

A review of flight data parameters downloaded from the airplane’s recoverable data module (RDM) revealed that the airplane’s autopilot was engaged for nearly the entire flight, from shortly after takeoff to about 17 seconds before the accident. The data showed that, after the controller cleared the flight for the approach, the airplane turned to the assigned heading vector, then it turned to a heading consistent with the final approach segment and began a descent toward the runway. When the airplane was about 200 ft msl (or about 117 ft agl) and about 0.4 nautical mile (nm) from the runway threshold with the flaps fully down, the autopilot was disengaged. The airplane’s pitch angle then increased rapidly to about 30° nose-up, its vertical ascent rate reached about 2,350 ft per minute (fpm), its flaps were reduced to 50%, and it climbed to about 450 ft msl, where it remained for about 2 seconds before it began to descend. The airplane then transitioned to an extreme nose-down pitch and extreme left-bank roll while its engine power increased. It briefly rolled back toward wings-level before again entering a left-bank roll, and its descent rate increased to about 4,000 fpm before the data ended. 

A witness outside at the airport stated that he heard the airplane’s engine noise go to full power, and, when he looked up, he saw the airplane in a sharp left turn before it descended to the ground. He stated that the weather conditions were “brutal” and that he could barely see the airplane at 200 yards away due to the thick fog. A witness who was driving a car near the airport captured video of the airplane in an uncontrolled descent, coming into view as it descended below a low cloud/fog layer.

The airframe was largely consumed by a postimpact fire that precluded a detailed examination of flight control continuity; however, all major components of the airplane were identified. Examination of the identified airframe components and the engine revealed no evidence of any preimpact malfunction, and a review of engine data parameters recovered from the RDM revealed that the engine operated normally throughout the flight. 

The autopsy of the pilot indicated cardiovascular disease that could be associated with increased risk of an impairing or incapacitating cardiovascular event such as heart attack or stroke. Although such an event cannot be excluded by autopsy evidence alone, there is no evidence that such an event occurred. Postmortem toxicology testing detected the opioid codeine, the codeine metabolite morphine, and thebaine. The presence of thebaine is not explained by pharmaceutical codeine use and likely indicates poppyseed consumption. It is possible that the measured codeine and morphine levels might be attributable to poppyseed consumption alone, although the possibility that codeine was also used cannot be excluded. Regardless, the codeine concentration in postmortem heart blood was low, and no morphine was detected in blood. As such, there is no clear evidence that the pilot was impaired by opioid effects at the time of the accident. Overall, there is no clear indication from reviewed evidence that the pilot was significantly impaired by effects of medical conditions or medications, but this possibility cannot be excluded given his identified risk factors for impairment.

The pilot’s logbooks were not recovered, so his total or recent experience flying in instrument meteorological conditions (IMC) was not known. Based on the available weather information, it is likely that the airplane was in IMC as the pilot descended on autopilot below the ILS approach decision height. The pilot’s subsequent actions while hand-flying the airplane, which included increasing the airplane’s pitch, reducing the flaps, and increasing engine power, were consistent with the initiation of a missed approach. 

Although vestibular illusions are commonly experienced by pilots during maneuvering flight in IMC, the accident pilot’s aggressive pitch control inputs while executing the missed approach likely intensified such vestibular illusions, increasing the likelihood of his experiencing spatial disorientation. The airplane’s subsequent extreme nose-down pitch and extreme left roll were consistent with the pilot’s loss of airplane control due to spatial disorientation.

- Probable Cause: The pilot’s aggressive pitch and power control inputs while executing a missed approach, which resulted in his spatial disorientation and a loss of airplane control.