Friday, April 03, 2026

Loss of control on ground: Piper PA-18-150 Super Cub, N3994Z, accident occurred on June 3, 2025, at Willow Airport (UUO/PAUO), Willow, Alaska

  • Location: Willow, Alaska 
  • Accident Number: ANC25LA071 
  • Date & Time: June 3, 2025, 09:30 Local 
  • Registration: N3994Z 
  • Aircraft: Piper PA-18-150 
  • Aircraft Damage: Substantial 
  • Defining Event: Loss of control on ground 
  • Injuries: 2 None 
  • Flight Conducted Under: Part 91: General aviation - Instructional

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/200508/pdf

https://data.ntsb.gov/Docket?ProjectID=200508

The flight instructor, seated in the rear seat, stated that he and the pilot receiving instruction, seated in the front seat, were practicing landings in a tailwheel-equipped airplane. The purpose of the flight was for the pilot that was receiving instruction to obtain a tailwheel endorsement.

During the landing rollout, gusting wind conditions lifted the left wing and the pilot receiving instruction applied right rudder, but the airplane continued to the right. The flight instructor then applied more right rudder; however, the airplane ground looped and sustained substantial damage to the right wing.

The instructor pilot reported that there were no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operation.

At the time of the accident, the pilot was landing on runway 13 with wind from 080° at 9 knots, gusting to 16 knots.

- Probable Cause: The flight instructor’s delayed remedial action/lack of supervision. Contributing to the accident was the pilot receiving instructions failure to maintain directional control during the landing roll in gusting wind conditions, which resulted in a ground loop.

Loss of control on ground: Temco GC-1B Swift, N78316, accident occurred on September 18, 2025, at South Lewis County Airport (TDO/KTDO), Toledo, Washington

  • Location: Toledo, Washington 
  • Accident Number: WPR25LA306 
  • Date & Time: September 18, 2025, 12:56 Local 
  • Registration: N78316 
  • Aircraft: Temco GC-1B 
  • Aircraft Damage: Substantial 
  • Defining Event: Loss of control on ground 
  • Injuries: 1 None 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/201817/pdf

https://data.ntsb.gov/Docket?ProjectID=201817

The pilot reported that as he prepared for takeoff in the tailwheel equipped airplane, he did not observe any movement of grass or trees due to wind. During the takeoff roll, the right wing rose suddenly, which the pilot counteracted with aileron inputs. The airplane bounced, and the right wing rose a second time, which the pilot counteracted. Subsequently, the airplane banked steeply to the left, exited the runway, and impacted the ground. The airplane sustained substantial damage to the fuselage, right aileron, and the elevator.

Prior to taxiing to and departing runway 24, the pilot observed a windsock, which indicated the wind was from about 260° at 2 to 6 knots. The airport manager reported there was a 20 knot crosswind at the time of the accident.

The pilot reported that there were no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation.

- Probable Cause: The pilot’s failure to maintain control of the airplane during takeoff in crosswind conditions.

Loss of control on ground: Maule M-7-235B Super Rocket, N116G, accident occurred on January 17, 2026, at Yellowstone Regional Airport (COD/KCOD), Cody, Wyoming

  • Location: Cody, Wyoming 
  • Accident Number: WPR26LA084 
  • Date & Time: January 17, 2026, 09:39 Local 
  • Registration: N116G 
  • Aircraft: Maule M-7-235B 
  • Aircraft Damage: Substantial 
  • Defining Event: Loss of control on ground 
  • Injuries: 5 None 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202316/pdf

https://data.ntsb.gov/Docket?ProjectID=202316

The pilot reported that during landing roll, the airplane began to move to the left, which he applied corrective control inputs to maneuver the airplane to the right. The pilot stated that as the airplane began to move to the right, it began to feel as if it was going to swing around. Subsequently, the left wing tip stuck the runway surface and the airplane swung about 270°, before it settled onto the right main landing gear, which collapsed. The airplane sustained substantial damage to the left wing, and both ailerons. At the time of the accident, the pilot was landing on runway 22 with calm wind.

The pilot reported no pre-accident mechanical failures or malfunctions with the airplane that would have precluded normal operation. 

- Probable Cause: The pilot's failure to maintain directional control during landing roll.

Landing area overshoot: Kitfox Series 7 Super Sport, N775DZ, accident occurred on January 19, 2026, near Lemmon Valley-Golden Valley, Nevada

  • Location: Lemmon Valley-Golden Valley, Nevada 
  • Accident Number: WPR26LA087 
  • Date & Time: January 19, 2026, 09:33 Local 
  • Registration: N775DZ 
  • Aircraft: Kitfox Series 7 
  • Aircraft Damage: Substantial 
  • Defining Event: Landing area overshoot 
  • Injuries: 1 Serious 
  • Flight Conducted Under: Part 91: General aviation - Personal 

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202327/pdf

https://data.ntsb.gov/Docket?ProjectID=202327

The pilot reported that he had performed a stop-and-go in a dirt clearing with a slight upslope. The pilot attempted to land in the clearing a second time, but during the landing flare, the pilot realized that he was going to land about 50 to 100 ft past his previous landing point and observed large sticks and a dirt mound in the available landing area ahead of the airplane. The pilot said that he initiated a go-around by applying full power and noted that he did not have the performance while in the low energy state. Subsequently, the landing gear briefly contacted the ground and the left wing dropped before the airplane impacted terrain. During the accident sequence, the left wing, left flaperon, and fuselage sustained substantial damage.

The pilot reported that there were no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation.

- Probable Cause: The pilot’s inability to maintain clearance from terrain during a go-around.

Thursday, April 02, 2026

Freedom Master FM-2 Air-Shark I, N220AS, fatal accident occurred on March 25, 2026, in Statesboro, Georiga

  • Location: Statesboro, GA 
  • Accident Number: CEN26FA147 
  • Date & Time: March 25, 2026, 14:53 Local 
  • Registration: N220AS 
  • Aircraft: Experimental Homebuilt Airshark 
  • Injuries: 1 Fatal 
  • Flight Conducted Under: Part 91: General aviation - Personal 

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202696/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N220AS

On March 25, 2026, about 1453 eastern daylight time, an experimental homebuilt Airshark airplane, N220AS, was substantially damaged when it was involved in an accident near Statesboro, Georgia. The pilot was fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91personal flight.

The airplane was being prepared for a ferry flight from Statesboro, Georgia, to Carrollton, Georgia, when one of the pilots decided to conduct a local flight to verify the airplane was performing normally before beginning the cross-country flight. Local authorities received a cell phone crash alert at 1453. First responders located the wreckage in a wheat field where it came to rest inverted.

The airplane struck a tree in about a 14° right wing low attitude about 42 feet above the ground on a 062° magnetic heading. A ground scar at 215 feet forward from the tree appeared to have been created by a propeller strike. At 218 feet from the tree, a large ground scar led up to the airplane which came to rest inverted 245 feet from the tree. An impression in the soil to the left of the large groundscar was consistent with the right wing as evidenced by the green position light lens found at the outer end of the impression.

An on site examination of the wreckage revealed no anomalies were found with the flight control system or flight control surfaces. Flight control continuity was verified for the ailerons, rudder, and elevators.

The airplane was reported to have been fueled to capacity (118 gallons) before the accident flight. The fuel selector in the cockpit was in the left fuel tank position. Both fuel tanks were breached, and the surrounding vegetation was yellow in the field where the wreckage came to rest. The right fuel cap and its receptacle were separated from the wing but present in the debris field next to the airplane. Both fuel caps were present and secure in their receptacles.

To facilitate viewing the fuel tank finger screens with a borescope, access holes were made in the wings near the wing root in the top wing skin. The right fuel tank finger screen was free of obstructions. The left fuel tank finger screen was corroded and appeared to be 30 to 40% obstructed. The obstruction’s appearance was consistent with solder used to manufacture the finger screen’s seam and end cap and did not appear to be foreign object debris from the fuel tank. Both fuel tanks were clean and free of debris in the area around the finger screens.

The airplane was equipped with a bail type gascolator and an inline paper element style fuel filter. The bail type gascolator bowl was sampled and blue liquid with an odor consistent with 100LL aviation fuel was collected in a container. When water-indicating paste was applied to the fuel, there was a small amount of water present (a tiny portion of the paste turned bright red). The gascolator bowl was removed and there was about a ½ teaspoon of water present. There was no filtering element or screen present in the gascolator bowl, and rust was present in the bottom of the bowl.

The paper style fuel filter was removed from its mount. It contained blue liquid consistent with the appearance and odor of 100LL aviation fuel. Water-indicating paste was added to the fuel. It did not indicate any water was present. The paper filter element was generally clean. Some rust and corrosion were present in the metal housing.

No leaks or anomalies were noted along the fuel lines in the airframe. Fuel was present in the engine compartment fuel lines and all the engine fuel system components examined. The fuel injector servo and fuel flow divider were disassembled and no anomalies were noted. The engine driven fuel pump was removed from the engine and produced air at the outlet port when it was actuated by hand. The unit was disassembled and no anomalies were noted.

The engine valve covers were removed and crankshaft continuity to the rear gears and to the valvetrain was confirmed. Compression and suction were observed from all six cylinders. A wire screen covered the fuel injector servo; corrosion and some trapped debris were present. No other induction air filtration system was present for this installation. Both magnetos exhibited impact damage. The left magneto did not produce spark when rotated by hand. The right magneto produced spark when it was rotated with a drill. The spark plug electrodes exhibited dark grey coloration and normal wear signatures. The No. 3 bottom spark plug electrodes were oil soaked. The ignition harness was secure and no damage was noted. Oil was observed in the engine. The oil suction screen contained about ¼ teaspoon of dark granular material. The oil filter was not examined due to impact damage.

The propeller remained attached to the engine. One blade was bent aft about 20° about 10 inches from its tip. One blade was curved aft about 50° about 12 inches from its tip. One blade was curved aft about 80° about 12 inches from its tip. All three blades were twisted in varying amounts towards their respective blade faces.

A Levil Flight Aviation broadcasting outer module (BOM) was found on the ground next to the airplane, which had been attached to one of the wing’s lower wing skin access covers. The unit is capable of providing flight data wirelessly to a phone or tablet in the cockpit when properly configured. The unit was reported to have been installed the day of the accident flight, but the contracted ferry flight pilot declined to configure the device due to time constraints. According to the manufacturer’s website, the unit may contain a flash memory card. The unit was retained for further examination.

Piper PA-28-140 Cherokee, N9913W, fatal accident occurred on March 20, 2026, near Whiteside County Airport (SQI/KSQI), Sterling, Illinois

  • Location: Rock Falls, IL 
  • Accident Number: CEN26FA141 
  • Date & Time: March 20, 2026, 15:03 Local 
  • Registration: N9913W 
  • Aircraft: Piper PA-28-140 
  • Injuries: 1 Fatal 
  • Flight Conducted Under: Part 91: General aviation - Instructional 

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202671/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N9913W

On March 20, 2026, about 1503 central daylight time, a Piper PA-28-140 airplane, N9913W, was destroyed when it was involved in an accident near Rock Falls, Illinois. The student pilot sustained fatal injuries. The airplane was being operated as a Title 14 Code of Federal Regulations Part 91 instructional flight.

The student pilot’s flight instructor stated that the student pilot arrived at the Whiteside County Airport (SQI) in Rock Falls, Illinois, around 1430 to complete his 10th solo flight since receiving his solo endorsement on February 12, 2026. According to the instructor the wind had been variable throughout the day and favored both runway 36 and runway 25 with windy conditions. The instructor stated that the student pilot was going to use runway 25 but was unsure what flight maneuver he was going perform for the local area flight.

At 1503, an automatic crash detection alert was received by local emergency services from the student pilot’s Apple iPhone. At 1510, first responders discovered the airplane upright in an agricultural field 1,100 ft south of runway 25. There were no witnesses who observed the accident.

The airplane came to rest upright on a heading of about 323°. The main debris field was about 36 ft in length on a heading of about 087° with the initial impact point ground scar containing fragments of the left wing tip and leading edge. A second impact ground depression was about 22 ft past the intimal impact point and contained forward fuselage debris. The left wing was separated from the airframe and found 67 ft past the initial impact point (see figure 1).


A secondary debris field extended past the airframe on a heading of about 087° and contained various baggage compartment items, sections of the cockpit instrument panel and interior, and personal items.

The right flap and flap control system were found in the full down position with the flap handle (Johnson bar) locked in that position. The flap handle was manipulated by hand and operated normally, however, the flap control cable between the bar and roller chain was jammed by impact damage and was unable to rotate the flap torque tube. Flight control continuity was established between all flight control surfaces and their respective cockpit controls. The elevator and aileron flight control cables had separations at the forward fuselage and spar box consistent with overload failure. The left pilot seat lap belt was found with the latch engaged but the left sidewall belt attachment pulled free from the airframe structure.

The engine crankshaft was rotated by hand by the propeller and continuity to the accessory section was established. The magnetos were removed and rotated with a drill with spark was observed on all leads. The engine driven fuel pump was also removed with fuel observed in the pump. The entire fuel system was found compromised and open to atmosphere in numerous locations consistent with impact damage. Fuel was only observed in the left fuel tank fuselage fuel line and the left wing fuel tank exhibited hydrologic deformation. No blockages were observed in the fuel lines, all fuel screens were clean, and the fuel selector operated normally.

The airplane was not equipped with an ADS-B Out transponder, and the Mode C transponder was found in the off position. The flight instructor stated that this was not unusual because the student pilot kept the radios off due to the airplane not being equipped with an avionics master switch.

A review of the student pilot’s logbook showed about 20 hours of recorded total flight time; 11.1 hours of dual instruction, and 3.8 hours of recorded solo time as of the logbook’s last entry on February 15, 2026. The flight instructor stated that the student pilot had flown an additional six solo and three dual instruction flights since February 15, 2026. Additionally, the student pilot had performed three unassisted takeoffs and landings with the flight instructor earlier in the day and the flight instructor had no concerns with him performing further solo flights.

A uAvionix Sentry ADS-B IN unit and an Apple iPhone were recovered and retained for further examination. 

Cessna 150G, N6305S, accident occurred on March 21, 2026, near Colorado Springs East Airport (CO4), Ellicott, Colorado

  • Location: Ellicott, CO 
  • Accident Number: CEN26LA156 
  • Date & Time: March 21, 2026, 10:23 Local 
  • Registration: N6305S 
  • Aircraft: Cessna 150G 
  • Injuries: 1 Serious 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202732/pdf

https://registry.faa.gov/aircraftinquiry/Search/NNumberResult?NNumberTxt=N6305S

On March 21, 2026, about 1023 mountain daylight time, a Cessna 150G airplane, N6305S, was substantially damaged when it was involved in an accident near Ellicott, Colorado. The pilot sustained serious injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported that he recalled completing a preflight inspection, a before takeoff engine run-up, and taxing onto the runway for takeoff. He did not recall any portion of the accident sequence.

A witness stated that the pilot intended to conduct some takeoffs and landings for currency. The pilot departed toward the south, and the takeoff appeared normal. The airplane went out of sight behind a hangar. However, when he regained sight of it, the airplane was on an easterly heading and in an approximate 60° left bank.

The airplane subsequently impacted the ground near wings level. It came to rest on a northeast heading about 100 ft before the departure end of the runway and about 500 ft left of the centerline. The airplane sustained damage to the fuselage, empennage, and both wings.  

Airframe and engine examinations are planned.