Tuesday, December 16, 2025

Piper PA-28R-201 Arrow III, N47700, fatal accident occurred on November 23, 2025, near Pittsfield, Illinois

  • Location: Pittsfield, IL 
  • Accident Number: CEN26FA049 
  • Date & Time: November 23, 2025, 21:37 Local 
  • Registration: N47700 
  • Aircraft: Piper PA-28R-201
  • Injuries: 1 Fatal, 2 Serious 
  • Flight Conducted Under: Part 91: General aviation - Personal
https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202036/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N47700

On November 23, 2025, about 2137 central standard time (all referenced times are CST), a Piper PA-28R-201 airplane, N47700, was substantially damaged when it was involved in an accident near Pittsfield, Illinois. The pilot was fatally injured, and the 2 passengers sustained serious injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

According to ADS-B flight track data, the pilot flew 4 flights on the day of the accident. The first leg was a 57-minute flight from Valkaria Airport (X59), Valkaria, Florida, to Tampa Executive Airport (VDF) between 0709 and 0806. The second leg was a 53-minute flight from VDF to X59 between 0903 and 0956. The third leg was a 4.25-hour flight from X59 to Anniston Regional Airport (ANB), Anniston, Alabama, between 1035 and 1450. The accident occurred during the fourth leg on a flight from ANB to Pittsfield Penstone Municipal Airport (PPQ), Pittsfield, Illinois.

According to available flight plan and weather briefing data, at 1602, the pilot filed an instrument flight rules (IFR) flight plan from ANB to Quincy Regional Airport (UIN), Quincy, Illinois, with a planned alternate of Southeast Iowa Regional Airport (BRL), Burlington, Iowa, and received a Leidos Flight Service standard weather briefing.

According to fueling documentation, after landing at ANB the pilot initially requested that the airplane be fueled with 40 gallons of fuel (20 gallons per wing fuel tank) but he subsquently amended his fuel request to only 36 gallons (18 gallons per wing fuel tank). According to the employee who fueled the airplane, the fuel level in each wing tank was below the 25-gallon indicator tab after the requested 18 gallons were added to each wing fuel tank.

According to the airplane’s engine data monitor, recorded data began at 1632:20 and the pilot selected takeoff power about 1642:33. At 1646:50, ADS-B flight track data began tracking the airplane flying to the northwest and in a climb. The airplane continued to the northwest toward UIN and climbed to a cruise altitude of 8,000 ft mean sea level (msl).

According to recorded air traffic control (ATC) transmissions, at 2025:13, the pilot contacted the Kansas City Center controller and reported being at 8,000 ft msl. At 2027:18, the controller asked the pilot if he had the current weather and notices to airmen (NOTAMs) at UIN, and which instrument approach the pilot intended to fly. At 2027:26, the pilot replied, “I’ve been looking at the weather at Quincy, it sounds like it’s, ah, fog, I am thinking about diverting to, ah, Pittsfield.” The controller then told the pilot that the current weather at UIN was 1.5 miles visibility with mist. At 2027:54, the pilot replied, “Okay, um, with one and a half miles visibility, yah, we can go into Quincy then.”

At 2028:02, the controller again asked the pilot which instrument approach at UIN he intended to fly. The pilot replied that he wanted to fly the RNAV Runway 22 instrument approach at UIN. At 2028:23, the controller cleared the flight direct to ALUGE which was the initial approach fix (IAF) for the RNAV Runway 22 instrument approach at UIN. At 2033:25, the controller cleared the pilot to descend at his discretion to maintain 4,000 ft msl.

At 2040:57, the controller told the pilot to cross ALUGE at or above 3,000 ft msl and cleared the flight for the RNAV Runway 22 instrument approach at UIN. At 2041:12, the controller asked the pilot to monitor the weather conditions during the descent and relay them to the controller.

At 2049:39, as the flight approached ALUGE, the controller told the pilot to change to advisory frequency and report when canceling IFR in the air or on the ground.

At 2101:59, the pilot told the controller that he was on the missed approach for the RNAV Runway 22 instrument approach at UIN. At 2102:40, the controller provided the local altimeter setting and asked the pilot to state his intentions. At 2102:56, the pilot told the controller that he wanted to divert to PPQ. At 2103:11, the controller cleared the flight direct to PPQ and to climb and maintain 3,000 ft msl. At 2104:40, the controller asked the pilot if he had an instrument approach request for PPQ. The pilot replied, “Ah, not yet.”

At 2107:25, the pilot transmitted over another pilot’s transmission but could be heard saying “we’re having engine troubles.” At 2107:35, the controller asked the pilot “what can I do for you?” The pilot did not respond. At 2107:46, the controller asked the pilot “how do you hear?” At 2107:50, the pilot replied to the controller “I hear you, but I don’t know where to head.” At 2107:53, the controller asked the pilot if he was having engine issues or if it was the weather conditions. The pilot did not reply. At 2109:07, the controller asked the pilot again if there was anything she could do to help. At 2109:12, the pilot replied, “it was a fuel issue, we are over onto the other tank, ah, we are heading back to, ah, Pittsfield, we would like, ah, RNAV 13, I believe it is.”

At 2110:48, the controller conveyed the 2055 weather report for PPQ, which was the current weather report provided to the ATC facility. The PPQ weather report was about 16 minutes old when the controller provided it to the pilot. At 2055, the PPQ weather consisted of wind 190° at 3 knots, 5 miles surface visibility, sky clear, temperature 5°, dew point 5°, and an altimeter setting of 30.16 inHg.

At 2111:10, the pilot replied, “if it’s clear I’ll just take 13 visual.” The controller told the pilot to report when he had PPQ in sight. The controller also relayed the current NOTAMS for PPQ, which consisted of an inoperative precision approach path indicator (PAPI) for runway 13 and two unlit towers north-northwest of PPQ.

At 2112:53, the controller cleared the flight to descend at pilot’s discretion to maintain 2,500 ft msl and she could not descend the airplane below 2,500 ft msl. At 2113:00, the pilot replied, “okay, [unintelligible] won’t go below two thousand five hundred, thank you.”

Postaccident review of available weather data established that the next PPQ weather report was issued at 2115 and, at that time, the general weather conditions at PPQ consisted of a clear sky and a 3-mile surface visibility.

At 2118:54, the controller asked the pilot if he had PPQ in sight. The pilot did not immediately reply. At 2119:16, the controller again queried the pilot. At 2119:21, the pilot replied, “we are still looking for Pittsfield, I think there’s fog in the area is what the issue is.” According to ADS-B flight track data, at that time, the airplane was descending through 2,100 ft msl and was about 1.8 nm north-northwest of the runway 13 threshold. 

At 2119:28, the controller told the pilot he had to climb back to 2,500 ft msl or she could not provide radar vectors for an instrument approach. At 2119:39, the pilot replied that he was climbing back to 2,500 ft msl.

At 2120:50, the pilot reported being at 2,500 ft msl and asked for radar vectors for the RNAV 13 instrument approach at PPQ. The controller told the pilot to turn left to 360°. At 2122:26, the controller cleared the flight direct to OMURE which was the IAF for the RNAV Runway 13 instrument approach at PPQ. At 2122:33, the pilot replied, “cleared direct to OMURE”.

At 2124:00, the controller told the pilot to cross OMURE at or above 2,700 ft msl and cleared the flight for the RNAV Runway 13 instrument approach at PPQ. At 2124:09, the pilot readback the crossing altitude and the instrument approach clearance.

At 2126:48, the pilot asked the controller if it would be possible to get radar vectors to GABDY which was the final approach fix (FAF) for the RNAV Runway 13 instrument approach at PPQ. At 2127:05, the controller told the pilot that the FAF was not depicted on her screen and that is why the flight was cleared to OMURE.

At 2127:24, the pilot told the controller, “I am little concerned on fuel, so, if you don’t mind if I cut the corner?” At 2127:29, the controller told the pilot, “You do whatever you think you need to do.” At 2127:33, the pilot replied, “Thank you.”

At 2128:32, the controller asked the pilot if he would like to change over to the PPQ advisory frequency or remain on the Kansas City Center frequency. At 2128:41, the pilot replied, “I would like to stay with you.”

At 2131:31, the controller told the pilot that he would have to cancel the IFR flight plan with Flight Service after he landed at PPQ. At 2131:39, the pilot replied, “Okay, we’ll do that.”

At 2134:43, the controller asked the pilot, “Is there anything that I can do to help?” At 2134:49, the pilot replied, “No, we’re, ah, lining up on final for a landing at, um, Pittsfield.” According to ADS-B flight track data, at that time, the airplane was descending through 2,975 ft msl and was about 0.9 nm northwest of the runway 13 threshold.

At 2134:56, the controller told the pilot that she still saw the flight at 3,000 ft msl over PPQ. At 2135:01, the pilot replied, “[unintelligible] losing altitude, I am at, ah, twenty six hundred.”

At 2135:15, the controller asked the pilot if he had the airport in sight. At 2135:21, the pilot replied, “Yes, we have the airport in sight.” At 2135:23, the controller approved the pilot to change to the PPQ advisory frequency and told him to cancel his IFR flight plan with Flight Service after landing. The pilot did not reply and there was no additional communication between the controller and the pilot for the remainder of the flight.

Postaccident review of available weather data revealed that the PPQ weather report issued at 2135 included a 300 ft above ground level (agl) overcast ceiling and a 0.75-mile surface visibility.

According to ADS-B flight track data, at 2135:28, the airplane crossed over PPQ midfield at about 1,935 ft msl, or about 1,234 ft agl, while it flew to the east-southeast. At that time, the airplane’s ground track was not aligned with runway 13. The airplane then turned north and flew away from PPQ.

According to engine monitor data, beginning at 2136:29, the engine power increased and remained above 95% until the end of the recorded data. At 2137:23, the last engine data was recorded with the engine running at 98% power, 2,680 rpm, 28.1 inHg manifold pressure, and 11.4 gph fuel flow. According to ADS-B flight track data, the airplane impacted an open cow pasture while in a left descending turn about 2 nm north of the runway 13 threshold at PPQ.

An onsite wreckage examination did not reveal evidence of a preimpact mechanical malfunction or failure that would have precluded normal operation of the airplane or its engine. Flight control cable continuity was confirmed from the cockpit to the respective flight control surfaces. The landing gear selector was found in the gear down position, and the flap selector handle was in the second flap detent position which corresponded to a 25° of wing flap extension.

The fuel selector was found in the right tank position. A functional check of the fuel selector valve confirmed its proper operation. The electric fuel pump switch was found in the ON position. The fuel lines were severed near each wing root during impact. About 0.5 gallon of uncontaminated 100 low lead aviation fuel was drained from the right wing fuel tank. About 1.3 pints of uncontaminated 100 low lead aviation fuel was drained from the left wing fuel tank.

The engine remained partially attached to the engine mount. Internal engine continuity and valve train continuity were confirmed while the crankshaft was rotated through the vacuum pump drive gear. Cylinder compression was confirmed by placing a finger over the open spark plug holes and feeling suction and expelled air from each cylinder while the crankshaft was rotated.

Both magnetos remained attached to the accessory housing. The magnetos drives were rotated by hand and spark was observed from all posts except one which exhibited impact-related damage to the harness wire. The sparkplugs exhibited normal wear signatures.

The fuel injection servo remained attached to the induction plenum. The throttle cable remained attached to the throttle lever, the throttle lever remained secure to the throttle arm with the serrated interface securely mated. The throttle arm was at the full throttle position. The mixture cable remained attached to the mixture lever, the mixture lever remained secure to the mixture arm with the serrated interface securely mated. The mixture arm was halfway between full rich and idle cutoff. The fuel line from the servo to the mechanical fuel flow gage was removed, and about 0.5 ounce of fuel was captured from the fuel line.

The engine driven fuel pump remained attached to the accessory housing and was safety-wired. About 0.75 ounce of fuel was present in the engine driven fuel pump. Fuel was present in the inlet to fuel pump line, but no fuel was present in the outlet to fuel injection servo line.

The flow divider remained attached to the crankcase spine with the individual fuel injection lines attached to the flow divider. Each fuel injection line remained secured to each fuel injection nozzle. The flow divider was removed from the engine, and fuel was present in the flow divider, there were no blockages observed, and the diaphragm was in a serviceable condition.

The vacuum pump remained attached to the accessory housing. Suction was observed while the vacuum pump drive was rotated by hand. The vacuum pump was disassembled, and no anomalies were observed to the internal vanes and core.

The propeller exhibited blade and hub damage that was consistent with rotation while under engine power. One propeller blade separated from the hub and exhibited a S-shaped spanwise bend, blade twisting toward low pitch, chordwise scoring of the blade face, and a fractured blade tip corner. The other propeller blade remained attached to the hub and exhibited a minor blade twist and leading-edge abrasions.

Review of the engine monitor data revealed that the airplane crashed about 4 hours and 55 minutes after it departed on the cross-country flight, the engine used about 46 gallons during the flight, and the average fuel consumption rate was about 9.3 gph. Additionally, the review of the engine monitor data did not reveal any evidence of a loss of engine power at the end of the flight.

A review of weather reports for nearby airports revealed visual meteorological conditions (VMC) existed to the east and north of PPQ at the time of the accident. Specifically, Mount Sterling Municipal Airport (I63), Mount Sterling, Illinois, located about 20 nm north of PPQ, and Jacksonville Municipal Airport (IJX), Jacksonville, Illinois, 26 nm east of PPQ, were both reporting a clear sky and 10-mile surface visibility at the time of the accident. Additionally, the airport listed as the planned alternate on the pilot’s IFR flight plan, Southeast Iowa Regional Airport (BRL), Burlington, Iowa, was also reporting a clear sky and 10-mile surface visibility at the time of the accident.

Socata TBM700C2, N700PT, fatal accident occurred on November 24, 2025, near Monroe Municipal Airport (EFT/KEFT), Monroe, Wisconsin

  • Location: Monroe, WI 
  • Accident Number: CEN26FA050 
  • Date & Time: November 24, 2025, 23:13 UTC 
  • Registration: N700PT 
  • Aircraft: Socata TBM 700 
  • Injuries: 2 Fatal 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202050/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N700PT

On November 24, 2025, about 1713 central standard time (CST), a Socata TBM 700 airplane, N700PT, was destroyed when it was involved in an accident near Monroe, Wisconsin. The pilot and pilot-rated passenger sustained fatal injuries. The airplane was operated as a Title 14 Code of Federal Regulations (CFR) Part 91 personal flight.

The airplane departed about 1641 CST from Oshkosh Wittman Regional Airport (OSH) in Oshkosh, Wisconsin. At 1704, according to an Air Traffic Control (ATC) communication recording, the airplane was cleared for the RNAV 12 approach at the Monroe Municipal Airport (EFT), Monroe, Wisconsin. At the time of the approach clearance, the 1655 automated weather observation at EFT reported wind from 180° at 6 knots, fog, ¼ statute mile visibility, overcast ceiling at 300 ft above ground level (AGL), and a temperature dewpoint spread of 0 degrees. The RNAV 12 approach Category A landing weather minimums were 400 ft AGL ceiling and 1 statue mile visibility. The pilot told ATC before the approach clearance that “if we can get in there it will be a full stop, if not we will go missed [approach] back to Oshkosh”. ATC gave the pilot an amended missed approach instructions of runway heading and 4,000 ft mean sea level (MSL). Prior to the pilot’s departure from OSH, the weather at EFT had been below the RNAV 12 landing minimums since 1215.

A witness at the airport reported that he heard the airplane increase engine power for a missed approach and he began searching for it in the fog. Shortly after the power up, he witnessed a bright orange glow and heard a loud explosion. Review of ADS-B data showed the airplane on a track of 121°, at an altitude of 1,500 ft MSL, and a ground speed of 110 knots crossing the RNAV 12 Visual Decent Point (VDP). The airplane then started a left turning climb to 1,800 ft msl to a track of 067° while increasing ground speed to 146 knots. The airplane continued to increase ground speed to 188 knots while entering a right turning decent to 1,100 ft MSL before starting a rapid right 270° climbing turn to an altitude of 3,000 ft msl (see Figure 1).


The airplane subsequently impacted mining equipment inside a gravel quarry about 0.5 nautical miles north of the airport. An initial impact point was the airplane’s right wing embedded in an elevated rock shaker table mounted on a semi-trailer (see Figure 2).


The airplane continued through another portable rock crusher and impacted a parked mine wheel loader which resulted in fragmentation of the airframe. Witness marks and impact damage on the portable mining equipment was consistent with a nose down high-speed impact. The debris field was about 300 ft in length and 200 ft in width on a heading of about 062° with evidence of an explosion and postaccident fire (see Figure 3).


Post accident examination of the debris field showed that the flaps and landing gear were in the retracted position. The PT6A-64 turboprop engine was found separated and fragmented through out the debris field. The turbine discs from the power section were located and found with all turbine blades fractured from the hub consistent with power at impact.

Review of FAA Aircraft Registration and insurance application records showed that the airplane was purchased by the pilot on November 4, 2025. Training records reviewed for both the pilot and pilot-rated passenger showed they had completed the insurance required TBM 700 Initial Training on November 5, 2025. Additionally, both the pilot and pilot-rated passenger held a private pilot certificate with an instrument rating and completed a flight review and instrument proficiency check on the same date. The pilot had previously owned a Cessna 421.

Two Garmin GTN 750s were located in the debris field and recovered for further examination. 

American Aviation AA-1A, N9439L, fatal accident occurred on November 26, 2025, near High Rolls, New Mexico

  • Location: High Rolls, NM 
  • Accident Number: WPR26FA051 
  • Date & Time: November 26, 2025, 11:45 Local 
  • Registration: N9439L 
  • Aircraft: American Aviation AA-1A 
  • Injuries: 2 Fatal 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202070/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N9439L

On November 26, 2025, about 1145 mountain standard time, an American Aviation AA-1A airplane, N9439L was destroyed when it was involved in an accident near Alamogordo, New Mexico. The pilot and passenger were fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot had recently purchased the airplane and received his private pilot certificate about one month prior to the accident.

On Nov 24, 2025, he began a long cross-country flight that departed Palm Beach County Park Airport (LNA), Palm Springs, Florida, about 1310. He flew to several destinations and landed at DeFuniak Springs Airport (54J), DeFuniak Springs, Florida, about 1843. On Nov 25, he departed 54J about 0921 and flew to several destinations and then landed at Cavern City Air Terminal (CNM), Carlsbad, New Mexico, about 2238.

The morning of November 26, 2025, the airplane departed CNM about 0702 and landed at Alamogordo-White Sands Regional Airport (ALM), Alamogordo, New Mexico, about 0803. About 1132, the airplane departed ALM and when the airplane did not return a concerned family member alerted authorities. The FAA then issued an Alert Notice (ALNOT) for the missing airplane. Subsequently, the airplane wreckage was located the next morning by the New Mexico State police about 7 miles east of ALM.

Preliminary flight track data was not available for the accident flight. The airplane came to rest on an ascending mountainous slope, at an elevation of about 6,300 ft mean sea level, on a heading of 150° magnetic. The rocky terrain was composed of downed trees, tree limbs, and loosely spaced pine trees that were about 75 ft in height. The first identified point of impact was the top of a tree, with several other severed tree branches. All major components of the airplane were contained within the accident site. Most of the airplane’s wreckage was consumed by a post impact fire.

The airplane was recovered to a secure facility for future examination.

Gray RG12, C-FGEW, accident occurred on November 26, 2025, at Southwest Michigan Regional Airport (BEH/KBEH), Benton Harbor, Michigan

  • Location: Benton Harbor, MI 
  • Accident Number: CEN26LA052 
  • Date & Time: November 26, 2025, 09:20 Local 
  • Registration: C-FGEW 
  • Aircraft: Gray RG12 
  • Injuries: 2 Minor 
  • Flight Conducted Under: Part 91: General aviation - Ferry

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202068/pdf

On November 26, 2025, at 0920 eastern standard time, a RG12 airplane, C-FGEW, sustained substantial damage when it was involved in an accident near Benton Harbor, Michigan. The pilot and a passenger sustained minor injuries. The airplane was operated under Title 14 Code of Federal Regulations as a Part 91 ferry flight.

The airplane was an experimental amateur-built replica of a Piper PA-12 that was being ferried by the pilot to the new airplane owner. About 10 minutes after the flight departed from Dowagiac Municipal Airport, Dowagiac, Michigan, an airframe vibration/flutter ensued. The vibration rapidly increased in severity despite changes in the airplane’s airspeed and engine power setting. During the flight, the ailerons contacted their mechanical stops, the horizontal stabilizer moved up and down vigorously, and the control stick was forced toward all corners of its travel range. The pilot decided to divert the flight to Southwest Lakes Airpark, Sawyer, Michigan, which had only one turf runway. After overflying the airstrip, the pilot decided it would be unsafe to attempt a landing due to the control issues and then flew to Southwest Michigan Regional Airport, Benton Harbor, Michigan, where he attempted a landing on runway 28 with winds from 240° at 27 knots gusting to 43 knots. The pilot stated that he was unable to obtain the latest wind information using his handheld radio because he was managing the control difficulties that were being experienced. The pilot stated that during landing, the airplane touched down on the main landing gear wheels, and he used full flight control inputs to counteract wind effects. During landing roll, the airplane veered right, the right wing contacted the runway, and the airplane nosed over. The airplane sustained substantial damage to the vertical stabilizer/rudder on impact with the runway surface.

Postaccident examination of the airplane revealed that the right wing drag and anti-drag wires were attached but found loose. Flight control continuity was established to all the flight controls.

Rutan Long-EZ, N82MT, accident occurred on November 19, 2025, near Beaufort, South Carolina

  • Location: Beaufort, SC 
  • Accident Number: ERA26LA052 
  • Date & Time: November 19, 2025, 16:30 Local 
  • Registration: N82MT 
  • Aircraft: TOOMEY Long EZ 
  • Injuries: 1 None 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202053/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N82MT

On November 19, 2025, about 1630 eastern standard time, an experimental, amateur-built Long EZ, N82MT, was substantially damaged when it was involved in an accident near Beaufort, South Carolina. The private pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The airplane departed the Chesapeake Regional Airport (CPK), Chesapeake, Virginia, at 1345, with an intended destination of Zephyrhills Municipal Airport (ZPH), Zephyrhills, Florida. Preliminary Automatic Dependent Surveillance-Broadcast (ADS-B) data obtained from the FAA showed that the airplane climbed to an altitude of 5,500 ft mean sea level (msl) after takeoff. Approximately 1 hour and 45 minutes into the flight, the airplane began a slow descent to 1,500 ft msl and at 1545, the airplane’s altitude fluctuated between 1,300 and 475 ft msl. The pilot reported that at approximately 1620, at an altitude of 1,500 ft above ground level (agl), the airplane’s engine began to run “extremely rough.” The pilot switched fuel tanks, applied carburetor heat, enriched the mixture, then leaned the mixture, turned on and off the auxiliary fuel pump, advanced and retarded the throttle, but the engine “ran progressively worse.” When the airplane was at approximately 500 ft agl, the engine lost all power, and the pilot performed a forced landing in a coastal tributary stream. The airplane sustained substantial damage to the fuselage and both wings.

The wreckage was retained for further examination.