Friday, August 29, 2025

North American T-28B Trojan, N28XT, fatal accident occurred on August 11, 2025, near Monticello, Iowa

  •  Location: Monticello, IA 
  • Accident Number: ANC25FA086 
  • Date & Time: August 11, 2025, 15:05 Local 
  • Registration: N28XT 
  • Aircraft: North American T-28B 
  • Injuries: 1 Fatal 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/200763/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N28XT

On August 11, 2025, about 1505 Central daylight time, a North American T-28B airplane, N28XT, was substantially damaged when it was involved in an accident near Monticello, Iowa. The pilot was fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

According to witnesses, the pilot reported, over the Monticello Regional Airport’s Common Traffic Advisory Frequency (CTAF), that he was experiencing a propeller governor failure, and he was returning to the airport. Shortly thereafter, he reported a total loss of engine power, and that he was attempting an emergency landing in a bean field about 2 miles Southeast of the airport (See figure 1).


During the subsequent emergency landing in the bean field, with the landing gear in the retracted position, the airplane continued along the wreckage path for about an additional 275 ft from the initial impact point.

The main fuselage, and associated debris path was oriented on about a 217° heading. The debris path between the initial impact point and the main wreckage site displayed signs of extensive fuselage fragmentation. Debris consisting of an engine oil tank and oil cooler, a propeller blade, and the accident airplane’s Wright R-1820 Cyclone 9 engine, were all found in the debris path. The airplane came to rest inverted, which resulted in substantial damage to the fuselage and wings (See figure 2).


An investigator from the National Transportation Safety Board's (NTSB) Alaska Regional Office, along with an NTSB aviation piston engine specialist, responded to the accident site and examined the airplane wreckage on August 12-14. During the detailed on-scene examination, the investigative team retained various components for additional examination and testing, and results are pending.

The wreckage has been moved to a secure site and additional postaccident examinations are pending. 

North American T-28C Trojan, N9748Y, accident occurred on August 7, 2025, near West Wendover, Utah

  • Location: West Wendover, NV
  • Accident Number: WPR25LA244 
  • Date & Time: August 7, 2025, 15:32 Local 
  • Registration: N9748Y 
  • Aircraft: North American T-28C 
  • Injuries: 2 Serious 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/200754/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N9748Y

On August 07, 2025, at 1532 Pacific daylight time, a North American T-28C, N9748Y, was substantially damaged when it was involved in an accident near West Wendover, Utah. The pilot and the passenger were seriously injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The passenger stated that they had arrived earlier in the week for Bonneville Speed Week and the purpose of the accident flight was to return home. Prior to departure they received full fuel, and the pilot started the engine, letting it run at idle while waiting for a helicopter to depart. They departed to the southeast and the pilot initiated a gradual climb. The pilot then began a right turn to head west toward mountainous terrain.

At an estimated 700–800 feet above ground level, the airplane began to shudder, which the passenger described as feeling the vibration emanating from the front of the airplane. He did not recall any reduction in power after takeoff, and he did not smell fuel, oil, smoke, or anything unusual, nor did he hear any abnormal sounds. As the shuddering worsened, the pilot continued the right turn, which the passenger interpreted as an attempt to return to the airport. When the airplane was heading back toward the airport, the vibration became severe.

The airplane descended and impacted the ground hard, bouncing several times before coming to rest about 1.5 miles from the airport. Dust immediately filled the cockpit, obscuring his view of the pilot. The pilot was bleeding from a head wound, but regained responsiveness after a couple of minutes. Both occupants had worn seat belts, but did not wear helmets.

The airplane was manufactured in 1956 by North American as model T-28C, and was designated serial number 140551. The airplane was powered by a Wright R1820-86B 9-cylinder radial engine rated at 1,425 horsepower and equipped with a Hamilton Standard 3-bladed constant speed propeller.

Investigators conducted a post-accident examination at the recovery facility. Oil had coated the left side of the airplane, with the origin at the engine breather tube (see figure 1 below). 

An external examination of the engine revealed no evidence of an uncontained failure. Oil was observed lightly coating cylinders Nos. 1, 2, 3, and 4. The No. 4 cylinder pushrods were bent with the pushrod housing nut on the exhaust valve displaced (see figure 2 below). 

Removal of the forward spark plugs revealed that cylinders Nos. 4, 6, and 7 were oil-soaked. The No. 6 forward spark plug was not torqued in the cylinder bore and was loose to rotate out of the cylinder. Investigators were unable to rotate the engine by applying force on the propeller blades. Investigators removed cylinder No. 4, providing an internal view of the crankcase. The articulating rods for Nos. 4, 5, and 6 were fractured at the master rod end. The corresponding cylinder skirts were damaged with grooves similar in dimension to the respective articulating rod, consistent with repeated contact between the skirt wall and the broken rod in the same plane. The articulating-rod journals on the master rod were not oil-covered (dry). The counterweights showed gouges on the outer portion of the shoe. Metallic debris was present on the aft side of the pistons and throughout the case.

The cylinder No. 4 articulating rod remained attached to the piston pin (see figure 3 below). The No. 4 piston face was dark with carbon, consistent with normal operation. The valves appeared normal with no evidence of piston-to-valve contact. The valve reliefs on the exhaust valve displayed a gouge consistent with the radius. The No. 4 piston was stuck in place and could not be freed.

The oil reservoir tank contained only a trace amount of oil with slight metallic debris on the bottom. The Cuno oil filter was removed and revealed fine metallic particles. The high-pressure oil strainer screen was removed and revealed coarser metallic particles (see figure 4 below). The metallic debris was both ferrous and non-ferrous, with mostly non-ferrous debris, indicative of aluminum, and there was additionally gold color flecks. The airplane was not equipped with an after-market “clean kit” or Whittaker valve, nor was it required.

The oil sump pump was removed; the gears were intact, and rotational scoring was noted on the gear vanes and surrounding housing with metallic particles present. The sump chip detector was coated with metallic particles. The chip detector on the supercharger had fine particles, but the screen was clean. Continuity was obtained on both chip detectors. The oil chip light in the cockpit was intact with no stretch noted in the filament. Continuity was obtained between the light and the cannon plug to the sump gear detector, indicating that it would have been operational. The oil shutoff poppet valve and spring on the oil pump housing appeared intact and operational.

Van's RV-6A, N692AC, accident occurred on August 19, 2025, near Centerview, Missouri

  • Location: Centerview, MO 
  • Accident Number: CEN25LA327 
  • Date & Time: August 19, 2025, 16:40 Local 
  • Registration: N692AC 
  • Aircraft: MARSHALL ALLEN L RV6A 
  • Injuries: 1 Minor, 1 None 
  • Flight Conducted Under: Part 91: General aviation - Personal 

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/200826/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N692AC

On August 19, 2025, at 1640 central daylight time, a Vans RV-6A airplane, N692AC, was substantially damaged when it was involved in an accident near Centerview, Missouri. The commercial pilot sustained minor injuries and the passenger was uninjured. The airplane was operated under Title 14 Code of Federal Regulations as a Part 91 personal flight.

The pilot stated there were no issues with the engine runup prior to the accident flight. He stated that this was his first flight in the make and model of accident airplane which was to familiarize himself with the airplane. After performing several maneuvers at 4,500 ft msl, he began to fly towards Skyhaven Airport (RCM), Warrensburg, Missouri. He said the engine sounded normal, but it was not producing power. He planned on continuing the flight to RCM where he now planned on performing a magneto check and to “recheck the engine.” About 3 miles from RCM, he performed the before landing checklist, changed the fuel tank selection, turned the fuel pump on, and confirmed the fuel mixture control was in the rich position. He reduced the throttle control about ¼ inches, heard a “slight pop,” and the engine lost power. He then changed the fuel tank selection, confirmed the fuel pump was on, and adjusted the engine throttle control, but was unable to regain engine power. He then changed fuel tank selection to the right fuel tank, added wing flaps, and performed a forced landing to a cornfield. He stated that the airplane, which was not equipped with a stall warning system, stalled above the corn during landing, and the airplane impacted the ground. The airplane sustained substantial damage to the fuselage.

The airplane was retained for examination.

Piper PA-18-150 Super Cub, N476SM, accident occurred on August 14, 2025, in Joliet, Illinois

"Yeah he can't park there" - Beau Klingbeil; FAA Inspector; Chicago, IL"

  • Location: Joliet, IL
  • Accident Number: CEN25LA322 
  • Date & Time: August 14, 2025, 17:14 Local 
  • Registration: N476SM 
  • Aircraft: Piper PA-18-150 
  • Injuries: 1 None 
  • Flight Conducted Under: Part 91: General aviation - Banner tow 

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/200810/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N476SM

On August 14, 2025, at 1714 central daylight time, a Piper PA-18-150 airplane, N476SM, was substantially damaged when it was involved in an accident near Joliet, Illinois. The pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 banner tow flight.

The pilot reported that he fueled the airplane and departed for a planned 3-hour banner tow flight in and around the Joliet area. About two hours into the flight, he heard a “loud bang” from the engine, which resulted in strong vibrations and a gradual loss of engine power. Shortly after, the engine experienced a total loss of power, and the pilot executed a forced landing to a field. During the landing roll, the airplane ground looped and impacted a fence, which resulted in substantial damage to the left elevator.

The responding FAA inspector reported that there was engine oil on the bottom of the fuselage from the engine cowling to the empennage. There was also oil leaking from the engine exhaust pipe.

Postaccident examination of the engine revealed that the No. 2 cylinder exhaust valve failed. Most of the valve stem remained inside the valve guide while the valve head was destroyed inside the cylinder. There were no other engine mechanical malfunctions or anomalies that would have precluded normal operation.  

Cirrus SR22 GTS G2, N412DJ, accident occurred on August 7, 2025, near Jaroso, Colorado

  • Location: Jaroso, CO
  • Accident Number: CEN25LA310
  • Date & Time: August 7, 2025, 09:35 Local
  • Registration: N412DJ
  • Aircraft: CIRRUS DESIGN CORP SR22
  • Injuries: 2 Serious, 1 Minor
  • Flight Conducted Under: Part 91: General aviation - Instructional

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/200736/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N412DJ

On August 7, 2025 at 0935 mountain daylight time, a Cirrus SR22 airplane, N412DJ, was substantially damaged when it was involved in an accident near Jaroso, Colorado. The pilot receiving instruction and a passenger were seriously injured, and the flight instructor was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 instructional flight.

The pilot reported that the purpose of the flight was to perform engine lean test procedures. During cruise flight at an altitude of 10,500 ft msl, the pilot reported they had already completed one lean test per the instructions and were starting a second test when the engine suddenly lost power. The instructor attempted to restart the engine by performing the emergency loss of engine power checklist but was unsuccessful in restarting the engine. They chose to activate the Cirrus Airframe Parachute System (CAPS) due to the lack of nearby airports. The CAPS deployed the parachute about 1,500 ft agl, and the pilot reported they were under canopy for about 20 seconds before the airplane landed hard which resulted in substantial damage to the fuselage and both wings.

The airplane was retained for further examination.

Van's RV-4, N595BS, accident occurred on August 6, 2025, near Elgin, Illinois

  • Location: Elgin, IL
  • Accident Number: CEN25LA309 
  • Date & Time: August 6, 2025, 19:25 Local 
  • Registration: N595BS 
  • Aircraft: Vans RV4 
  • Injuries: 2 None 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/200735/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N595BS

On August 6, 2025, about 1925 central daylight time, a Vans RV4 airplane, N595BS, was substantially damaged when it was involved in an accident near Elgin, Illinois. The pilot and passenger were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 as a personal flight.

The pilot reported that during cruise flight at 1,000 ft above ground level, he noticed an increase in electrical voltage. He turned the airplane toward the departure airport and noted the voltage indicated 20 volts before the entire instrument panel lost power, and then the engine lost power. He also noticed a small smoke plume from behind the instrument panel. The pilot made a forced landing to a golf course during which the airplane sustained substantial damage to the fuselage and engine mount.

The engine was equipped with two E-Mag electronic ignition systems. Both magnetos were retained for further examination.

Devices capable of recording data were sent to the NTSB Vehicle Recorders Laboratory for further analysis.

The airplane was retained for further examination.

Rockwell Commander 112A, N112EF, accident occurred on July 23, 2025, at Patrick Leahy Burlington International Airport (BTV/KBTV), Burlington, Vermont

  • Location: Burlington, VT 
  • Accident Number: ERA25LA292 
  • Date & Time: July 23, 2025, 13:00 Local 
  • Registration: N112EF 
  • Aircraft: ROCKWELL INTERNATIONAL 112 
  • Injuries: 1 None 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/200747/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N112EF

On July 23, 2025, about 1300 eastern daylight time, N112EF, a Rockwell International 112 airplane, was substantially damaged when it was involved in an accident near Burlington, Vermont. The pilot was not injured. The flight was conducted under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight.

The pilot/owner departed Patrick Leahy Burlington Airport (BTV), Burlington, Vermont, about 0840, with 48 gallons of fuel, and flew to Martha’s Vineyard Airport (MVY), Martha’s Vineyard, Massachusetts. He landed about 1020. The pilot said that he planned to purchase fuel in MVY, but the wait was too long and departed back to BTV about 1104. The pilot stated that he was on the downwind leg of the airport traffic pattern for runway 10 at BTV when the engine suddenly lost power. He attempted to reach the runway but landed about 15 ft short and impacted a berm resulting in substantial damage to the left wing spar.

The airplane wreckage was retained for further examination.

Grumman G-164B AgCat, N8834H, accident occurred on July 1, 2025, near Lockport, Louisiana

  • Location: Lockport, LA 
  • Accident Number: CEN25LA231 
  • Date & Time: July 1, 2025, 11:45 Local 
  • Registration: N8834H 
  • Aircraft: GRUMMAN ACFT ENG CORSCHWEIZER G-164B 
  • Injuries: 1 None 
  • Flight Conducted Under: Part 137: Agricultural
https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/200448/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?NNumberTxt=N8834H

On July 1, 2025, about 1145 central daylight time, a Grumman G-164B airplane, N8834H, was substantially damaged when it was involved in an accident near Lockport, Louisiana. The pilot received minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 137 aerial application flight.

The pilot reported that on the morning of the accident he had flown two previous aerial application flights in the accident airplane without issue. The outside air temperature and humidity had increased since the first two flights. During the accident flight the airplane contained about 35 gallons of fuel and about 160 gallons of liquid applicant in the hopper. The pilot descended into the target field and completed one spray pass. As he approached the end of the field he ascended and “noticed the plane not climbing as normal.” The engine gauges all showed normal indications, but the airplane would not turn or climb as expected. The airplane descended as he approached a highway, and he did not want to dump the hopper over the highway or the adjacent bayou, so he continued forward. The airplane cleared a set of powerlines next to the highway and landed hard in a field, then nosed over. The pilot egressed the airplane without further incident.

The responding FAA inspector reported that the airplane came to rest inverted in a field. The engine and propeller were mostly separated from the firewall. The upper and lower wings remained attached to the fuselage and sustained leading edge damage.

The airplane has been retained for further examination.

Piper PA-24-250 Comanche, N7412P, accident occurred on August 28, 2025, near Richmond Field Airport (69G), Gregory, Michigan

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N3806Y

- Hitstory of Flight:
On August 28, 2025, at about 1548 local time, a Piper PA-24-250 Comanche, N7412P, registered to Espyess Aviation LLC out of Sylvania, Ohio, was destroyed when it was involved in an accident near Richmond Field Airport (69G), Gregory, Michigan. The sole pilot onboard sustained serious injuries. The personal flight originated from Charlevoix Municipal Airport (KCVX), 
Charlevoix, Michigan, and was destined to Lambertville-Toledo Suburban Airport (KDUH), Lambertville, Michigan.

According to preliminary automatic dependent surveillance-broadcast (ADS-B) data, at 1439 LT, the airplane departed runway 27 at KCVX and proceeded to an inflight cruising altitude of 4,900 ft. At about 1546:15, the airplane entered a descent towards 69G. At 1546:55, the airplane conducted a right turn. At 1547:36, the airplane entered a tight descending 270 turn towards the south runway (runway 36) at Richmond Field. The last ADS-B return was recorded at the end of the turn as the aircraft was descending through 1150 ft, 60 knots groundspeed, with an average rate of -700 feet per minute (fpm). (figure 1)

Figure 1: ADS-B Exchange with Google Earth Pro

The airplane impacted trees and open field terrain short of the runway and was consumed by a post crash fire. The wreckage consisted of the entire airplane, which came to rest upright about 0.30 miles from the approach end of runway 31. Both wings and tail remained attached to the airframe. Downed trees near the airplane suggests it descended into trees in a wings level and nose level altitude. One propeller blade was visible in published photos from the accident site, the damage to the propeller suggests it was making little to no power on impact.

The accident aircraft, serial number 24-2600, was manufactured in 1961. It featured an all-metal monoplane of semimonocoque construction with tricycle retractable landing gear a single-engine and 4 seats. It was powered by a Lycoming O-540 reciprocating 250 hp engine.

Richmond Field Airport is a public airport located 2 miles southeast of Gregory, Michigan. It features a single turf runway 18/36 which is 2471 x 100 ft. The airport field elevation was 921 ft.

The reported weather at KOZW, at 1535 (about 13 minutes before the accident) included: wind 340° at 5 knots, 10 statute miles visibility, a scattered (SCT) ceiling at 2,700ft AGL, a broken (BKN) ceiling at 3,800ft AGL and 6,000ft AGL, a temperature of 22° C, a dew point of 15° C, and a barometric altimeter setting of 30.02 inches of mercury. The calculated density altitude was 1869 ft.

The reported weather at KOZW, at 1555 (about 7 after before the accident) included: wind 300° at 7 knots, 10 statute miles visibility, a scattered (SCT) ceiling at 2,900ft AGL, a broken (BKN) ceiling at 3,600ft AGL and 4,800ft AGL, a temperature of 22° C, a dew point of 14° C, and a barometric altimeter setting of 30.01 inches of mercury. The calculated density altitude was 1879 ft.