Saturday, November 08, 2025

Extra EA 300/SC, N330SL, fatal accident occurred on November 8, 2025, at Keystone Heights Airport (42J), Keystone Heights, Florida

This is preliminary information, subject to change, and may contain errors. Any errors in this post will be corrected when the preliminary report is released.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N330SL

- History of Flight:
On November 8, 2025, at about 1040 local time, an Extra EA 300/SC, N330SL, registered to Avtech Group LLC out of St. Augustine, FL, was destroyed when it was involved in an accident at Keystone Heights Airport (42J), Keystone Heights, Florida. The sole pilot onboard sustained fatal injuries. The local flight originated from 42J.

Preliminary information indicates the airplane was conducting aerobatic manoeuvres when it entered an inverted spin and lost control.

Preliminary ADS-B data shows that the airplane was flying over the airport at 3,700 ft when it entered a sudden descent to 1,000 ft and disappeared from coverage.

- Pilot Information:
unknown at this point.

- Airplane Information:
The accident aircraft, serial number SC050, was manufactured in 2014. It was a single-seat, low-wing aerobatic monoplane powered by a Lycoming IO-580-X engine rated at 320 hp.

According to the Pilot Operating Handbook (POH):
The plane is designed for acrobatics. Inverted flight maneuvers are limited to max 4 min.

Figure: POH Information

According to section 4.12.3, SPIN:
To enter a spin proceed as follows: 

  • Reduce speed, power idle 
  • When the plane stalls: 
  1. kick rudder to desired spin direction 
  2. hold ailerons neutral 
  3. stick back (positive spinning), Stick forward (negative spinning)

The plane will immediately enter a stable spin. 

  • Ailerons against spin direction will make the spin flatter. 
  • Ailerons into spin direction will lead to a spiral dive. 

Above apply for positive and negative spinning. 

To stop the spin: 

  • Apply opposite rudder 
  • Make sure, power idle 
  • Hold ailerons neutral 
  • Stick to neutral position
After one turn of spinning the plane will recover within about 1/2 turn. 

After six turns of spinning the plane will recover within about 1 turn. 

Recovery can still be improved by feeding in in-spin ailerons. 

N O T E
If ever disorientation should occur during spins (normal or inverted) one method always works to stop the spin: 

  • Power idle 
  • Kick rudder to the heavier side (this will always be against spin direction) 
  • Take hands off the stick The spin will end after 1/2 thru 1 turn. 

The plane will be in a steep dive in a side-slip. Recovery to normal flight can be performed easily. 

N O T E 
After one turn of spinning the altitude loss including recovery is within about 1500 ft. 
After six turns of spinning the altitude loss including recovery is within about 3300 ft.

- Wreckage and Impact Information:
The airplane impacted open flat terrain, came to rest inverted and was consumed by a post crash fire. The main wreckage consisted of the entire airplane, which was confined within one area without a notable debris field. Both wings and tail remained attached to the airframe. It appears that both propeller blades remained attached to the propeller hub, which was still attached to the engine. The impact appears consistent with an inverted flight profile with little to no forward airspeed.

- Airport Information:
Keystone Heights Airport is a non-towered public airport located about 3 miles north of Keystone Heights, Florida. The airport field elevation was 196 ft. The airport features two asphalt runways, runway 5/23 (5046x100 ft) and runway 11/29 (4899x75 ft).

- Weather:
The reported weather at 1035: Winds 180 at 5 knots, visbility 9 miles, a broken cloud layer at 8500 ft, temparture 25°C, dewpoint 19°C, and an altimeter setting of 29.95 inches of mercury

METAR K42J 081515Z AUTO 19004KT 8SM FEW080 FEW090 24/19 A2995 RMK A01
METAR K42J 081535Z AUTO 18005KT 9SM BKN085 25/19 A2995 RMK A01 <<<
METAR K42J 081555Z AUTO VRB04KT 9SM OVC085 25/19 A2994 RMK A01

- Additional Information:
On

Runway excursion: Boeing 737-823 (WL), N991AN, incident occurred on February 10, 2024, at Dallas/Fort Worth International Airport (DFW/KDFW), Dallas, Texas

  • Location: Dallas, Texas 
  • Incident Number: DCA24LA095 
  • Date & Time: February 10, 2024, 19:42 Local 
  • Registration: N991AN 
  • Aircraft: Boeing 737-823 
  • Aircraft Damage: Minor 
  • Defining Event: Runway excursion 
  • Injuries: 104 None 
  • Flight Conducted Under: Part 121: Air carrier - Scheduled

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/193772/pdf

https://data.ntsb.gov/Docket?ProjectID=193772

On February 10, 2024, about 1942 central standard time, American Airlines flight 1632, a Boeing 737-823, N991AN, experienced a brake system anomaly after landing on runway 17L at the Dallas-Fort Worth International Airport (DFW), Dallas-Fort Worth, Texas. The airplane came to a stop in the paved overrun area beyond the south end of the runway threshold. All 104 passengers and crew members safely evacuated the airplane via airstairs, with no injuries reported. The flight was operated as a scheduled domestic passenger service under the provisions of Title 14 Code of Federal Regulations (CFR) Part 121, traveling from Ronald Reagan Washington National Airport (DCA), Arlington, VA, to DFW in Dallas-Fort Worth, TX.

Analysis:

American Airlines flight 1632 experienced a brake system anomaly shortly after landing on runway 17L at Dallas-Fort Worth International Airport (DFW), Dallas-Fort Worth, Texas. The anomaly resulted in a loss of braking effectiveness that increased the airplane stopping distance. The airplane came to a stop in the paved overrun area beyond the south end of the runway threshold. The crew executed emergency procedures, including engine shutdown and auxiliary power unit (APU) activation, ensuring a safe post-incident response. All 104 passengers and crew members safely evacuated the airplane via airstairs, with no injuries reported. The flight was operated as a scheduled domestic passenger service under the provisions of Title 14 Code of Federal Regulations (CFR) Part 121, traveling from Ronald Reagan Washington National Airport (DCA), Arlington, VA, to DFW.

Each main landing gear (MLG) has a normal braking system powered by hydraulic system B and manually controlled by the flight crew via brake pedals in the flight deck. Pedal movement is transmitted through cables to left and right brake metering valves located in the wheel well, which regulate hydraulic pressure to the respective brake assemblies. Each wheel is equipped with a rotor-stator brake assembly that uses hydraulic pressure to generate braking force.

On February 6, 2024—four days before the incident—American Airlines completed a scheduled modification on the airplane, replacing the original steel brakes with carbon brakes and associated wheel assemblies. This work was performed in accordance with an Engineering Order (EO) and associated cards dated November 2, 2022, based on Boeing Service Bulletin SB 737-32-1429, Revision 4. The modification applied to Boeing 737-800 series airplane equipped with Goodrich or Honeywell steel brakes and wheels. The EO and associated cards included detailed maintenance instructions with sign-off blocks and incorporated the technical content of the Boeing Service Bulletin, supplemented with additional information to ensure compliance with American Airlines’ continuous airworthiness maintenance program.

As part of the conversion to carbon brakes, four flow limiters were installed, replacing the existing bulkhead unions between the rigid hydraulic tubes and flexible hydraulic hoses. Due to the increased length of the flow limiters, the original rigid tubes (four total) located inboard of each MLG within the wing were replaced with shorter ones. Installation required temporary disconnection of each flexible hose, removal of the bulkhead union, installation of the flow limiter, and reconnection of the flexible hose.

Flight data recorder (FDR) data recorded brake pressure from two transducers—one for each side—located upstream of the antiskid valves. These transducers reflect hydraulic pressure supplied by the autobrake system or the pilot-controlled metering valves during manual braking. The recorded values during the incident appeared consistent with expected inputs, indicating no upstream braking system issues. However, the FDR does not record data downstream of the transducers, limiting the ability to evaluate antiskid valve functionality or overall brake system performance. Additional parameters such as wheel speed and brake pressure at the assemblies would enhance investigative capabilities.

The flight crew indicated that they selected an autobrake setting of 3 for the landing at DFW. The autobrake system supplies metered brake pressure to help decelerate and stop the airplane after landing or if a rejected takeoff (RTO) occurs. It monitors airplane deceleration and controls metered pressure to maintain the target deceleration rate selected by the pilot on the AUTO BRAKE select switch until the airplane comes to a full stop, provided there is no flight crew input. Available settings include RTO, OFF, 1, 2, 3, and MAX.

FDR data indicated that both the autobrake system and ground spoilers were functioning at the onset of the landing roll. Upon landing, the increase in the hydraulic brake pressures were consistent with the autobrake setting 3. However, manual brake application by the flight crew likely occurred within seconds of the autobrake application, overriding the autobrake system. The autobrake application discrete parameter confirmed the autobrake was applied for one sample, approximately one second. Once the flight crew’s manual brake application overrode the autobrake, the flight crew controlled the brakes for the remainder of the landing rollout.

According to Boeing, the autobrake system disengages when the metered brake pressure reaches or exceeds 750 pounds per square inch (PSI). During this landing, the right brake pressure increased steadily from 0 to 3000 PSI within four seconds; the left brake pressure increased to 3000 PSI within ten seconds. At the time of autobrake disengagement, the right brake pressure was increasing past 750 psi. This data suggests that a crew member manually applied brakes resulting in the autobrake system disengaging.

Post-incident troubleshooting revealed that the flexible hydraulic hoses connected to the number 3 (right inboard) and number 4 (right outboard) MLG brakes had been improperly reconnected following the carbon brake and flow limiter installation. Specifically, the flexible hydraulic hoses supplying pressure to the number 3 and 4 brakes had been swapped at their connections with the flow limiters (see figure 1).

Further system troubleshooting by American airlines revealed a discrepancy with the wiring to the left MLG wheel speed transducers. During an operational test, maintenance personnel discovered that the wiring harness within the MLG axle had been installed incorrectly. Specifically, the electrical connectors for the number 1 (left outboard) and number 2 (left inboard) wheel speed transducers were swapped.

As a result of these two discrepancies, when a skid occurs, the non-skidding wheel would receive the brake pressure release intended for the wheel on the same MLG that is skidding, and the skidding wheel would receive the (potentially full) metered brake pressure due to its brake not being released. This is because the skidding wheel would receive the antiskid commands intended for the non-skidding wheel, and vice versa.

Given the combination of the switched hydraulic brake hoses and wheel speed transducers, the use of manual braking would not have released the subsequently locked and skidding outboard tires. Eventually, the skidding tires were worn flat until the tires failed. The failed tire would lead to lost braking effectiveness that increased the airplane’s stopping distance beyond the end of the runway.

The investigation confirmed that the only mechanical discrepancies were the reversed hydraulic hoses to the number 3 and number 4 MLG brakes and the reversed wheel speed transducer wires for the number 1 and number 2 MLG wheels.

Safety Actions

American Airlines subsequently revised engineering order card 3222J004-001 adding a step to label the flexible hydraulic hoses prior to removal and requiring an inspector to verify the flexible hydraulic hoses are properly re-installed. In addition, the transducer operational test was incorporated into engineering order card 3222J004-001. This operational test is capable of detecting either swapped flexible hydraulic hoses or swapped transducer connectors.

Additionally, American Airlines issued engineering authorizations (EA) and engineering orders to check the entire B737 fleet for swapped transducer wiring. A total of 50 airplanes were inspected by EA and 253 airplanes were inspected by EO. Of all 303 airplanes inspected, zero were found with transducer wiring swapped. American Airlines also revised their B737NG and MAX aircraft maintenance manuals (AMMs) to enhance the transducer operational test and the main landing gear installation job card has been updated with enhanced steps to ensure the transducer wires are not crossed.

Following the incident, Boeing added Information Notice 02 to service bulletin 737-32-1429 Revision 4. This notice was distributed to alert operators to the risk of crossing hydraulic hoses when reconnecting the flexible hydraulic hoses to the new flow limiters. The notice emphasizes that each flexible hydraulic hose must be reconnected to its corresponding flow limiter and that hoses must not be crossed at any point along their length. Improper reconnection – such as attaching a flexible hydraulic hose to the incorrect flow limiter – will result in incorrect antiskid system operation, potentially leading to a loss of braking action and/or tire failure.

Additionally, Boeing has issued two Fleet Team Digests - 737MAX-FTD-32-24002 and 737NG-FTD-32-24001 - to provide both interim actions as well as final actions to B737NG and B737MAX operators. The interim actions include a list of best practices such as

o Temporarily labeling flexible hydraulic hoses to the corresponding brake positions,

o Labeling wiring harnesses when disconnecting wheel speed transducers, and

o Functional checks to verify flexible hydraulic hoses and transducer wiring is correctly connected. 

The final actions include revising specific AMM tasks and service bulletins where improper maintenance may occur. Boeing released Service Bulletin 737-32-1429 Revision 5 on August 14, 2025. Furthermore, Boeing issued SB 737-32A1599 on October 14, 2025, to ensure proper hydraulic routing following the implementation of service bulletins that alter brake configurations.

The NTSB has investigated several aircraft incidents and accidents that have been the result of cross wiring of wheel speed transducers, all were the result of maintenance human error.

- Probable Cause: Improper maintenance due to human error during a braking system modification diminished braking performance. Contributing to the diminished braking performance was the lack of a functional check to verify the flexible hydraulic hoses and transducer wiring were connected correctly after the braking system modification.

Friday, November 07, 2025

Socata TBM700C2, N111RF, fatal accident occurred on October 13, 2025, in Dartmouth, Massachusetts

  • Location: Dartmouth, MA 
  • Accident Number: ERA26FA011 
  • Date & Time: October 13, 2025, 08:15 Local 
  • Registration: N111RF 
  • Aircraft: Socata TBM 700 
  • Injuries: 2 Fatal, 1 Minor 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/201836/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N111RF

On October 13, 2025, at about 0815 eastern daylight time, a Socata TBM 700C2, N111RF, was substantially damaged when it was involved in an accident near Dartmouth, Massachusetts. The private pilot and the passenger were fatally injured and an automobile driver received minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

According to preliminary air traffic control ADS-B and voice communication data provided by the Federal Aviation Administration, the pilot had filed an instrument flight rules flight plan from New Bedford Regional Airport (EWB), New Bedford, Massachusetts, to the Kenosha Regional Airport (ENW), Kenosha, Wisconsin. The airplane departed EWB at 0805, and shortly after departure, the pilot stated that he would be returning to the airport. The air traffic controller then instructed the pilot to enter a left downwind for runway 05, an instruction which the pilot confirmed. The controller then queried the pilot if he would need assistance upon landing, to which the pilot reported that he did not need assistance. The controller then cleared the pilot to land on runway 05. 

The controller next asked the pilot whether he could perform an approach to the airport and reported that the ceilings were around 1,000 ft, or if he would need radar vectors. The pilot responded that he would descend and that he “should be OK.” The controller acknowledged the pilot and cleared him again to land on runway 05. About one minute later, the controller provided the pilot with a low altitude alert and the altimeter setting that was current at the time. The pilot confirmed the altimeter setting. Shortly after, the pilot made an unintelligible exclamation. There were no further communications from the pilot. 

The accident site was located about 3.6 nautical miles southwest of EWB. Several trees that were impact-damaged were identified as the initial impact points. The trees had the tops cut off approximately 50 feet above the ground. The wreckage path continued through a wooded area, across a highway off ramp, across a portion of Interstate 195 West, and the fuselage came to rest in the median between Interstate 195 West and Interstate 195 East. During the impact sequence, the airplane impacted an automobile that was traveling on Interstate 195 West and the driver received minor injuries. The distance from the initial impact point to where the fuselage came to rest was about 280 ft. The debris path was oriented along a heading of 223° true, and the fuselage came to rest oriented on a heading of 289° true. A post-impact fire consumed portions of both wings and the empennage. All of the major components of the airplane were located at the accident site.

Both wings were impact damaged, and portions of both wings had been partially consumed by a post-impact fire. The left aileron was located along the wreckage path and the aileron trim tab remained attached. The rudder sustained significant impact damage to the leading edge, and a portion of the rudder had broken free from the rest of the rudder. The rudder trim tab remained attached to the rudder through its hinge; however, the rudder trim actuator had separated from the rudder trim tab; the damage was consistent with impact. The elevator trim tab remained partially attached to the elevator through the trim tab actuator and the trim tab and both elevators were impact and thermally-damaged.

The wing fuel tanks were breached, and no fuel was recovered from the remnants of the fuel tanks; however, there was a strong odor consistent with Jet A fuel noted around the accident site. The fuel strainer bowl and screen remained secured, and there were no signs of fuel leaks. The bowl was removed, and the screen was clear of obstructions. The fuel contamination indicator was in its normal position. The fuel line connecting the fuel outlet at the firewall to the fuel pump inlet was secure and there were no signs of fuel leaks.

The fuselage was the furthest piece of wreckage observed along the wreckage path and remained mostly intact; however, the fuselage structure was buckled in multiple locations, and there was a small portion of thermal damage to the forward left side of the fuselage. A portion of the left wing root remained attached to the fuselage, the right wing had completely impact-separated from the fuselage. The main cabin door was found open when the investigators arrived; however, a witness video that was taken after the accident showed that the cabin door was closed immediately after the accident. Both forward seats had impact-separated from their installation points and remained within the cabin area.

The airplane was equipped with a digital avionics suite. Both the pilot and copilot primary flight displays (PFD) remained installed, and the electrical connectors remained secured. Both flight displays were recovered and retained for data download.

The engine remained partially attached to the airframe through the engine mounts, cables, wires, and hoses. The engine displayed some impact damage signatures and there were no signs of fire.

The five blade, constant speed, composite propeller sustained impact damage to all five blades. The propeller blade hub remained attached to the propeller flange. All five of the propeller blades had separated from the propeller hub near their roots, and all of the propeller blades were located along the wreckage path. The blades displayed varying amounts of leading-edge damage.

The wreckage was retained for further examination.
  • Conditions at Accident Site: IMC 
  • Condition of Light: Day Observation Facility, Elevation: EWB,79 ft msl 
  • Observation Time: 08:16 Local 
  • Distance from Accident Site: 3.6 Nautical Miles 
  • Temperature/Dew Point: 13°C /12°C 
  • Lowest Cloud Condition: 
  • Wind Speed/Gusts, Direction: 19 knots / 28 knots, 40° Lowest Ceiling: Broken / 900 ft AGL 
  • Visibility: 2.5 miles 
  • Altimeter Setting: 30.04 inches Hg 
  • Type of Flight Plan Filed: IFR 
  • Departure Point: New Bedford, MA (EWB) 
  • Destination: Kenosha, WI

Mooney M20E Super 21, N79338, fatal accident occurred on October 31, 2025, near Saratoga County Airport (5B2), Saratoga, New York

  • Location: Ballston Spa, NY 
  • Accident Number: ERA26FA027 
  • Date & Time: October 31, 2025, 10:35 Local 
  • Registration: N79338 
  • Aircraft: Mooney M20E 
  • Injuries: 1 Fatal, 1 Serious 
  • Flight Conducted Under: Part 91: General aviation - Personal
https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/201941/pdf

https://registry.faa.gov/aircraftinquiry/Search/NNumberResult?NNumberTxt=N79338

On October 31, 2025, about 1035 eastern daylight time, a Mooney M20E, N79338, was destroyed when it was involved in an accident near Ballston Spa, New York. The pilot was fatally injured, and the flight instructor was seriously injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

According to the flight instructor, the pilot had just purchased the airplane and he was going to fly with the pilot to Punta Gorda, Florida, where the pilot lived. The insurance company required the pilot to fly with a flight instructor due to the pilot’s lack of experience in the airplane make and model. 

The flight instructor stated that he met the pilot for the first time the night before the accident, and they discussed the airplane’s maintenance issues and planned flight route. The flight instructor added that the pilot had test flown the airplane about 1 month prior to the accident flight. He also stated that the airplane’s engine lost power during the pilot’s test flight and that he had landed safely back at the airport at he end of that flight. The flight instructor described that the airplane’s fuel had been contaminated with algae and debris. A local mechanic subsequently repaired the fuel tank and cleaned out the fuel system. 

On the day of the accident flight, the flight instructor and pilot performed a preflight inspection of the airplane and sampled fuel from the fuel tanks several times before departing. The flight instructor stated that after takeoff and during the initial climb, about 200 ft above ground level, the engine decreased in power from 2,500 rpm to about 1,500 rpm. A few seconds later the engine decreased to about 500 rpm and then lost all power. The flight instructor took over control of the airplane and tried to make a turn back to the airport. When he made a right turn, he realized that the airplane was too low. He then made a slight left turn to avoid a house before the airplane impacted a tree.

The accident site was located in a subdivision beside a house. The airplane impacted a tree about 20 ft up, fell to the ground, and came to rest oriented on heading of 232° magnetic. The engine was fractured off its mounts and lying beside the fuselage. The propeller was still attached to the engine and did not display s-bending, leading edge gouging, or chordwise scratching. All major components of the airplane were located at the accident site. A postimpact fire consumed portions of the engine, instrument panel and cockpit. No useful information was obtained from the remaining instrumentation.

The right wing root was still attached to the fuselage and about 6 ft of the outboard portion of the wing was located in a tree directly above the main wreckage. The aileron was still attached to the outboard portion of the wing. The right flap remained attached to the wing. The flaps were in the full retracted position. The left wing also remained attached to the fuselage. The wing was consumed by fire, and the left fuel tank was destroyed. The flap was attached to the wing. About 3 ft of the outboard portion of the left wing fractured off the wing and was located about 20 ft from the main wreckage. The left wing had several tree impressions down the leading edge. The cockpit, instrument panel, and engine bay were destroyed by fire. No useful information was obtained. The tail section was attached to the empennage. The left stabilator and elevator were bent up mid-span. The rudder and right elevator were unremarkable. 

The airplane was further examined after it was recovered from the accident site. Flight control continuity was visually established through torque tubes and fracture surfaces consistent with impact damage. The fuel system from the pickup tubes to the engine fuel injectors was clear of debris and air was passed through all lines and valves. The system exhibited no blockages or other abnormalities.

The engine rocker box covers, engine driven fuel pump, magnetos, and the remnants of the airframe baffling were removed. The crankshaft was rotated by applying hand pressure to the propeller, and after the start ring gear and propeller collar were removed, full 360° rotation of the crankshaft was achieved. Compression and suction were observed on all four cylinders, normal valve action was observed on all cylinders, the accessory idler gears were observed rotating, and mechanical continuity was confirmed throughout. The cylinders were examined with a boroscope. Oil pooling was observed in the No. 2 and No. 4 cylinders, and all cylinders were clean with very little deposits on the piston faces or combustion domes. The induction plenum was inspected via borescope and no blockage or obstructions were observed. All four induction tubes remained attached to the engine with various levels of impact-related damage. The exhaust system remained secure to the engine and was partially crushed from impact forces. It was inspected via borescope and no blockage was observed.

The fuel flow divider remained secure to the crankcase spine. All four fuel injection lines remained secure to the flow divider, and to their respective fuel injection nozzles. The fuel inlet line remained secure to the flow divider. The flow divider and lines were removed and the flow divider was disassembled. The diaphragm was brittle and destroyed consistent with exposure to extreme heat, and no blockage was observed in the flow divider. Air was blown through the inlet fitting and was observed coming out of all four injection nozzle lines. All four fuel injection nozzles were removed and oil was present in the No. 2 and No. 4 nozzles (oil likely from the orientation of the engine after the accident). The oil was blown out and no contamination was observed in any of the fuel injection nozzles. All four of the nozzles had the restrictor inserts installed. Air was blown through the flow divider inlet fuel line and fuel flow transducer, no obstructions observed. 

The engine-driven fuel pump remained attached to the engine accessory housing with the fuel inlet and outlines secure to it. The fuel inlet line had been cut during the engine recovery process. The engine driven pump was removed; it did not create inlet suction and outlet pressure when the lever was actuated. The pump was disassembled, the diaphragms were brittle and destroyed consistent with exposure to extreme heat. The fuel pump was filled with engine oil. 

The left and right magnetos remained secure to the engine accessory housing with the harness caps secure to the magnetos. The magnetos were removed and both drives were found secure via castle nut and cotter pin. The left magneto’s drive was not free to not rotate. While the right magneto’s drive rotated, no spark was observed. Both of the magnetos displayed thermal damage consistent with exposure to the postimpact fire. 

About 6 gallons of fuel was removed from the right wing fuel tank. The fuel was blue in color and smelled like 100LL fuel. No water or debris was found in the right fuel tank. The left fuel tank was consumed by fire.

  • Conditions at Accident Site: VMC 
  • Condition of Light: Day
  • Observation Facility, Elevation: SCH,378 ft msl 
  • Observation Time: 10:49 Local
  • Distance from Accident Site: 20 Nautical Miles 
  • Temperature/Dew Point: 11°C /0°C
  • Lowest Cloud Condition: 
  • Wind Speed/Gusts, Direction: 19 knots / 28 knots, 280°
  • Lowest Ceiling: Overcast / 2600 ft AGL 
  • Visibility: 10 miles
  • Altimeter Setting: 2922 inches Hg 
  • Type of Flight Plan Filed: NONE
  • Departure Point: Ballston Spa, NY 
  • Destination: Punta Gorda, FL (PGD) 

Air Tractor AT-502, N7315L, accident occurred on November 5, 2025, near Gueydan, Louisiana

This is preliminary information, subject to change, and may contain errors. Any errors in this post will be corrected when the preliminary report is released.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N7315L

- History of Flight:
On November 5, 2025, at about 1430 local time, an Air Tractor AT-502, N7315L, registered to Coco Aviation LLC out of Plaucheville, LA, sustained substantial damage when it was involved in an accident near Gueydan, Louisiana. The sole pilot onboard sustained serious injuries. The Part 137 agricultural flight originated from a private location in 
Plaucheville, Louisiana.

Source: NTSB CEN26LA036, event type assigned as "Collision with terr/obj (non-CFIT)," suggesting it was most likely a powerline strike.

Landing gear not configured: Cessna R182 Skylane RG, N9054C, accident occurred on November 5, 2025, at Brainerd Lakes Regional Airport (BRD/KBRD), Brainerd, Minnesota

This is preliminary information, subject to change, and may contain errors. Any errors in this post will be corrected when the preliminary report is released.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N9054C

- History of Flight:
On November 5, 2025, at about 1330 local time, a Cessna R182 Skylane RG, N9054C, sustained substantial damage when it landed gearup on runway 34 at Brainerd Lakes Regional Airport (BRD/KBRD), Brainerd, Minnesota. The sole pilot onboard was not injured. The local flight originated from KBRD.

Source: NTSB CEN26LA038

Wildlife encounter (non-bird): Cessna 172M Skyhawk, N9490H, accident occurred on November 4, 2025, at Grantsburg Municipal Airport (GTG/KGTG), Grantsburg, Wisconsin

This is preliminary information, subject to change, and may contain errors. Any errors in this post will be corrected when the preliminary report is released.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N9490H

- History of Flight:
On November 4, 2025, at about 1830 local time, a privately-registered 
Cessna 172M Skyhawk, N9490H, sustained substantial damage when it struck an animal (type unknown) during a landing attempt at Grantsburg Municipal Airport (GTG/KGTG), Grantsburg, Wisconsin. The sole pilot onboard was not injured. The airplane climbed out and landed at Burnett County Airport (RZN/KRZN), Siren, Wisconsin. The flight originated from Ely Municipal Airport (ELO/KELO), Ely, Minnesota, at about 1643 LT, and was destined to KRZN.

The NTSB the investigating the event as an accident (case number CEN26LA035) and reported the type of event as "Wildlife encounter (non-bird)."