Saturday, July 26, 2025

Aircraft structural failure: Wittman Buttercup, N18263, fatal accident occurred on May 28, 2023, near Lyndonville, New York

  • Location: Lyndonville, New York
  • Accident Number: CEN23FA204 
  • Date & Time: May 28, 2023, 18:15 Local 
  • Registration: N18263 
  • Aircraft: Luce Buttercup 
  • Aircraft Damage: Destroyed 
  • Defining Event: Aircraft structural failure 
  • Injuries: 2 Fatal 
  • Flight Conducted Under: Part 91: General aviation - Personal
https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/192250/pdf

https://data.ntsb.gov/Docket?ProjectID=192250

On May 28, 2023, at 1815 eastern daylight time, an experimental, amateur-built Luce Buttercup, N18263, was destroyed when it was involved in an accident near Lyndonville, New York. The pilot and pilot-rated passenger sustained fatal injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.


The pilot, who was the owner and builder of the experimental, amateur-built airplane, departed with a pilot-rated passenger on a 15 to 20-minute local flight. Witnesses reported that the airplane broke up in flight and descended to the ground. The debris path extended for about 1,435 ft, beginning with debris from the wings, consistent with failure related to the wing structure.

Postaccident examination of the engine and propeller revealed no mechanical anomalies that would have precluded normal operation. No preimpact flight control deficiencies were found. There was no evidence of flutter. The wing separations were consistent with upward and aft bending and/or torsional loading based on deformation signatures of the wing attachment brackets, strut brackets, and front strut attachment fittings (outboard end). Fracture surfaces of the wing attachment brackets and front strut fittings were consistent with overstress separation. No flight track information was available for the accident flight.

The pilot built the airplane based on dimensions from another airplane for which no plans had been produced. The accident airplane was issued a special airworthiness certificate about 21 years before the accident. At the time of the accident, the airplane had been modified from its original configuration with the installation of a heavier, higher horsepower engine and the installation of a different propeller. Because no maintenance records were located for the airplane, there was no information available regarding this modification, the airplane’s operational time, or its inspection/maintenance history.

The airplane’s design/build plans were not based upon a structural engineering analysis to determine a structural design envelope, structural loads, or structural performance.

Accordingly, the basis for any design safety margins and limitations are unknown. There were no regulatory design requirements for the airplane due to its experimental classification. 

Metallurgical examination revealed no conclusive evidence of pre-existing or progressive damage signatures that would have initiated the accident, and fractured structural components were consistent with overstress separation. One small area of possible fatigue fracture was observed emanating from the weld face on the lower-forward left strut end fitting at the outboard end; however, based on the amount of deformation observed in this area, it was not a likely fracture initiation point.

The pilot’s toxicological testing detected several volatile solvents; however, the volatile solvent levels measured in the pilot’s tissues cannot be used to reliably predict the route of his exposure or specific effects. Thus, whether the pilot had inhaled volatile solvents recreationally or was experiencing any impairing effects of volatile solvent exposure, could not be determined. Toxicological testing also detected ethanol in liver tissue; n-butanol (a potential indicator of postmortem microbial activity) was also detected in this specimen; however, it is likely that the detected ethanol was from sources other than alcohol consumption and did not likely contribute to the accident.

The pilot’s toxicology results also demonstrated the presence of central nervous system depressant medications, including cyclobenzaprine and gabapentin. Cyclobenzaprine use may be associated with significant performance impairment. Use of gabapentin can also increase the user’s somnolence, dizziness and fatigue, potentially impairing pilot performance. Both cyclobenzaprine and gabapentin have potential postmortem redistribution; therefore, reliably associating levels with impairing effects is not possible. Overall, whether the pilot’s use of cyclobenzaprine and gabapentin contributed to the accident cannot be determined.

The pilot-rated passenger’s mild-to-moderate coronary artery disease conveyed some increased risk of a sudden impairing or incapacitating cardiac event, including angina, arrhythmia, or heart attack. There is no autopsy evidence that such an event occurred. However, such an event does not leave reliable autopsy evidence if it occurs immediately before death. The aircraft was configured such that it could be controlled from either the left or right front seat. Thus, it is unlikely that the pilot-rated passenger’s coronary artery disease contributed to the accident.

In addition, the pilot-rated passenger’s toxicological testing indicated use of citalopram and diazepam. Citalopram and diazepam, and conditions that may be treated with these medications, can adversely affect pilot performance and judgment. However, it is unclear if the pilot-rated passenger’s performance or judgment were a factor in the outcome; whether effects of the pilot-rated passenger’s use of citalopram and diazepam or of any associated underlying conditions contributed to the accident cannot be determined.

Although the available information is consistent with an in-flight failure of the wing structure due to overload, given the lack of flight track information or recorded data from onboard the airplane, the circumstances of the in-flight breakup could not be determined. 

- Probable Cause: An in-flight breakup due to structural overload of the airplane for undetermined reasons.

Fuel related: Cessna 182D Skylane, N8775X, fatal accident occurred on May 28, 2023, near Plymouth, New York

  • Location: Plymouth, New York
  • Accident Number: ERA23FA249
  • Date & Time: May 28, 2023, 14:52 Local 
  • Registration: N8775X 
  • Aircraft: Cessna 182 
  • Aircraft Damage: Substantial 
  • Defining Event: Fuel related 
  • Injuries: 1 Fatal 
  • Flight Conducted Under: Part 91: General aviation - Skydiving
https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/192249/pdf

https://data.ntsb.gov/Docket?ProjectID=192249

On May 28, 2023, about 1452 eastern daylight time, a Cessna 182D, N8775X, was substantially damaged when it was involved in an accident near Plymouth, New York. The commercial pilot was fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 skydiving flight.

The pilot departed on the third skydiving flight of the day with four skydivers on board and climbed to about 11,000 ft mean sea level (msl) when the jumpers departed the airplane. The pilot flew back to the airport and reported over the common traffic advisory frequency (CTAF) that he was descending through 6,000 ft msl. The operator reported hearing the pilot make another radio call on the CTAF but the “…call did not sound like a normal one and I could not identify what he said. I thought by the sound of his voice something was off.' A witness heard the engine sputtering followed by the engine losing power and then heard the impact. The airplane impacted trees and terrain about 1 nautical mile from the center of the intended airport, coming to rest in a nose-low, tail-high attitude with the left wing separated at the wing root.

Postaccident examination of the flight controls revealed flight control continuity, and all fractures were consistent with overload. The examination of the engine revealed crankshaft, camshaft, and valvetrain continuity. The air induction, exhaust, lubrication systems, magnetos, and spark plugs revealed no evidence of preimpact failure or malfunction. The carburetor heat was found in the off position.

Postaccident examination of the airframe revealed that the right-wing fuel bladder was intact and contained about 25 ounces of fuel. The left-wing fuel bladder was breached; there was no evidence of significant fuel leakage from the ruptured left-fuel tank evidenced by minimal fuel blight of the vegetation in the immediate area. There was no evidence of fuel siphoning aft of either wing-tank fuel filler cap. The fuel selector was found in the left-tank detent. No fuel was found in the left- or right-inlet fuel lines or the outlet line of the fuel selector valve. No fuel stains were noted on the interior panel below the fuel selector valve. About 5 ounces of fuel were drained from the airframe fuel strainer and about 4 ounces were found in the carburetor bowl. 

The pilot fueled the airplane the day before by adding 30.3 gallons of 100 low lead fuel. The amount of fuel in the airplane before he added the fuel is unknown. He then flew two uneventful skydiving flights that day. The operator reported that on the next day the pilot flew another skydiving flight in the morning, and when the pilot returned from the flight, he checked the fuel level with a dipstick and stated that he had 40 gallons of fuel on board. The operator reported that the pilot had enough time to refuel the airplane but chose not to. The pilot flew another skydiving flight before the accident flight, which was the fifth flight since he fueled the airplane the day before. The operator reported the airplane burned 7 to 9 gallons of fuel per skydiving flight. 

The pilot used a fuel dipstick to assist in determining the fuel level in the tanks. However, the fuel dipstick used was not made for the make and model of the accident airplane. Therefore, a fuel conversion chart was created to indicate how much fuel was actually in the tank when the dipstick was used. If the airplane had 40 gallons of fuel on board as the pilot stated, there should have been enough fuel for the intended flight. However, had the pilot misinterpreted the fuel dipstick reading, he may have believed he had about 43 gallons of fuel on board, as indicated by the dipstick, when instead there were about 24 gallons, as indicated by the conversion chart. In that case, during the next three flights, the airplane could have sustained fuel exhaustion as a result of the fuel burn and the unusable fuel in each tank. 

The nearest weather station, located about 29 miles from the accident site, indicated the temperature and dew point spread was 27°C and 8°C, respectively, which was conducive for carburetor icing at glide or cruise power. About 1443, ADS-B data indicated that the airplane began its descent from about 11,000 ft msl and 3 minutes later it descended through 6,000 ft msl, about a 1,666 ft-per-minute rate of descent. The last ADS-B radar point was about 1450, and the airplane was about 1,500 ft msl. 

While the pilot had a history of diabetes being treated with a medication and a documented history of retinopathy, it is unlikely that the pilot had symptoms of severe high or low blood glucose at the time of the accident. Minor symptoms of diabetes, such as fatigue or blurry vision, could not be entirely excluded. Due to his heart disease, the pilot was at significantly increased risk of a sudden impairing or incapacitating cardiac event, including angina, arrhythmia, or heart attack. There is no autopsy evidence that such an event occurred; however, such an event does not leave reliable autopsy evidence if it occurs immediately before death.

It is possible that the pilot's report of the fuel level using the dipstick did not account for the fuel conversion chart that would have indicated that the airplane had about 24 gallons of fuel on board, and not the reported 40 gallons. In this scenario, the pilot would have departed on the flight with substantially less fuel than anticipated, and the engine lost power due to fuel exhaustion. 

However, the evidence supports another possible scenario: the airplane was descending from about 11,000 ft msl and at a high rate of descent in atmospheric conditions that were conducive to carburetor icing in cruise and glide power. The carburetor heat was found in the off position after the accident. Had the pilot not used carburetor heat during the descent, it is also possible that the engine sustained a complete loss of engine power due to carburetor icing.

Accordingly, the definitive cause of the total loss of engine power could not be determined.

- Probable Cause: A total loss of engine power for reasons that could not be determined.

Friday, July 25, 2025

Piper PA-25 Pawnee, N8186K, fatal accident occurred on July 12, 2025, near Hot Springs, South Dakota

  • Location: Hot Springs, SD 
  • Accident Number: CEN25FA248 
  • Date & Time: July 12, 2025, 13:22 Local 
  • Registration: N8186K 
  • Aircraft: Piper PA-25 
  • Injuries: 1 Fatal 
  • Flight Conducted Under: Part 91: General aviation - Glider tow

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/200517/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N8186K

On July 12, 2025, about 1322 mountain daylight time, a Piper PA-25, N8186K, was substantially damaged when it was involved in an accident near Hot Springs, South Dakota. The pilot was fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 glider aerotow flight.

The pilot of the glider being aerotowed reported that the accident occurred during his fourth flight of the day and a pre-takeoff briefing was performed before each aerotow. The glider pilot stated that on the accident flight, after liftoff, he kept the glider in a standard tow position while he contended with updrafts until the glider reached 1,500 ft agl at which point the glider was in a higher-than-normal tow position. The glider pilot radioed the towplane pilot that he was going to release from the tow rope. The glider pilot reportedly pulled the glider’s tow rope release knob twice but did not feel the rope disconnect. He subsequently determined the glider had separated from the tow rope, and he made an otherwise uneventful landing at the airport on runway 19.

A witness reported that the towplane and glider were in a climbing left turn and were about 500 to 600 ft agl when the glider appeared to get “extremely high” on the aerotow. The towplane pitched down, and the glider appeared to release from the tow rope. According to the witness, the towplane never recovered from the nose down attitude before it impacted terrain.

The towplane impacted terrain about one mile north of the departure end of runway 6 at the Hot Springs Municipal Airport, Hot Springs, South Dakota. The towplane accident site was located on an embankment of a gravel pit, and a postaccident fire ensued. The airplane impacted terrain in an estimated 50° nose-down pitch attitude. The relative angle between the airplane at impact and the 30° sloped embankment was about 100°.  The glider tow rope with a metal ring on each end was found at the accident site. The tow rope was about 200 ft in length and was constructed of a yellow hollow braid polypropylene rope.

All primary flight control surfaces and flaps were accounted for at the accident site and remained attached to their respective attachment points. All flight control cables were found attached to their respective flight control surfaces.

The towplane’s tow rope release latch and associated release cable were continuous from the cockpit to the latch mechanism at the tail. The latch was found in the open position, and the tow rope attachment ring was found on the ground about 15 ft from the latch. The rope extended in a south direction from the wreckage with portions suspended from tree branches. The towplane’s latch functioned normally when functionally tested.

The fixed 2-blade propeller remained attached to the engine crankshaft propeller flange. One blade exhibited an S-shaped bend and twisting near the blade tip. The leading edge exhibited leading edge polishing and chordwise scratch marks on the camber side. The other blade exhibited chordwise scratch marks on the camber side. Both blades had gouges in the leading edges. The cockpit throttle position was found to be near the idle power position, and the correlating throttle arm on the carburetor was found to be at the idle stop. The carburetor heat control arm was found in the off position. The mixture control was found in a mid-range setting. The engine crankshaft was rotated by turning the propeller by hand. No anomalies were found with the engine that would have precluded normal operation.

The glider came to rest in the grass next to the runway. A portion of yellow rope with a metal ring attached, consistent with a “weak link” portion of a glider tow rope, was found directly under the glider. This 7 ft long section of tow rope was found with a metal ring on one end and a broom straw separation on the eye splice end, as seen in figure 1. The metal ring was found directly under the glider’s tow hook latch.

The glider was moved to a hangar for further examination. During the examination, the tow hook release knob required about 22 lbs of force to release the latching mechanism. The sound of the release cable binding in its metal conduit was heard as the release handle was moved through its full travel (forward and aft). The latch mechanism otherwise functioned normally. An exemplary glider tow hook release knob was tested and required about 4 lbs of force applied to release the latching mechanism without any audible cable binding.

The towplane was recovered from the accident site to a secure location.

Cessna 182G Skylane, N3261S, accident occurred on July 3, 2025, near Kona, Hawaii

  • Location: Kona, HI
  • Accident Number: ANC25LA063
  • Date & Time: July 3, 2025, 06:57 Local 
  • Registration: N3261S 
  • Aircraft: Cessna 182G 
  • Injuries: 1 Minor 
  • Flight Conducted Under: Part 91: General aviation - Positioning

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/200461/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N3261S

On July 3, 2025, about 0657 Hawaii-Aleutian standard time, a Cessna 182G airplane, N3261S, was substantially damaged when it was involved in an accident near Kona, Hawaii. The pilot sustained minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 positioning flight.

The pilot reported that the flight was a repositioning flight from the Upolu Airport (UPP), Hawi, Hawaii to the Kona International Airport (KOA). The pilot said that the airplane had 21 gallons of fuel on board. He sumped the fuel tanks before departure and the fuel was clean, and the predeparture engine run up checks were all normal.

The pilot said that while en route to KOA at 2,400 ft msl, he maintained a cruise power setting of 2,300 rpm and 22 inches of manifold pressure. However, during the approach for landing at KOA, about a half mile away, and before the pilot began to adjust the airplane to a landing configuration, he noticed the Engine Gas Temperatures (EGTs) were higher than expected at a full rich mixture setting and concluded that the engine was running lean. The pilot confirmed no loss of manifold pressure and ruled out carburetor icing. Subsequently the engine began to lose power. The pilot applied carburetor heat, and the engine began to run better for about 15 to 20 seconds before the engine lost all power. The pilot selected an area of rough, uneven, lava-covered terrain as a forced landing site, which resulted in substantial damage to the fuselage and wings.

A detailed engine examination is pending the recovery of the wreckage.

Thursday, July 24, 2025

Faust 3, N5901V, accident occurred on June 30, 2025, near Harrison, Montana

  • Location: Harrison, MT 
  • Accident Number: WPR25LA200 
  • Date & Time: June 30, 2025, 12:00 Local 
  • Registration: N5901V 
  • Aircraft: FAUST 3 
  • Injuries: 2 None 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/200471/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N5901V

On June 30, 2025, about 1200 mountain daylight time, an experimental amateur built Faust 3, N5901V, sustained substantial damage when it was involved in an accident near Harrison, Montana. The pilot and passenger were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported that he was performing a water landing in the float equipped airplane on Willow Creek Reservoir near Harrison. Shortly after touch down, the airplane pulled to the left. The wings subsequently struck the water before the airplane came to a stop, which resulted in substantial damage to both wings.

The airplane was recovered from the water and retained for further examination. 

Cessna 182B Skylane, N7166E, accident occurred on July 4, 2025, at Belen Regional Airport (BRG/KBRG), Belen, New Mexico

  • Location: Belen, NM 
  • Accident Number: WPR25LA207 
  • Date & Time: July 4, 2025, 09:00 Local 
  • Registration: N7166E 
  • Aircraft: Cessna 182B 
  • Injuries: 3 None 
  • Flight Conducted Under: Part 91: General aviation - Personal 

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/200514/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N7166E

On July 4, 2025, about 0900 mountain daylight time, a Cessna 182B, N7166E, was substantially damaged when it was involved in an accident near Belen, New Mexico. The pilot and two passengers were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

According to the pilot, during the takeoff roll, the airplane became airborne prematurely, when the airspeed indicator displayed 40 knots. They thought it was due to ground effect, and leveled the airplane to gain airspeed, however, the indicated airspeed did not increase. The pilot stated that while in ground effect, the airplane’s ground speed increased, and the airplane “felt” like it wanted to climb. Near the end of the available runway, the pilot concluded that the airspeed indicator was not displaying correctly, and was unsure how fast the airplane was flying, and initiated a climb, as the airspeed continued to indicate 40 knots. The pilot remained within the airport traffic pattern for runway 03, and while on downwind, noticed the indicated airspeed rose to 60 knots, then while on final, it had reduced to 40 knots. During landing, the airplane bounced and subsequently landed hard on the nose landing gear.

Post accident examination of the airplane revealed substantial damage to the forward fuselage and engine mount.

The wreckage was retained for further examination.

Kitfox 3, N422K, accident occurred on July 22, 2025, at Logan-Cache Airport (LGU/KLGU), Logan, Utah

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed.

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N422K

On July 22, 2025, at about 1640 local time, a privately-registered Kitfox 3, N422K, sustained substantial damage when it was involved in an accident at Logan-Cache Airport (LGU/KLGU), Logan, Utah. The pilot was not injured, and passenger sustained minor injuries. The flight originated was originating at the time.

The FAA reported that the aircraft "lost control on takeoff, veered off runway and gear collapsed" from runway 10/28.

The winds at the time were from 200° at 11 knots, gusting 17 knots.

- Weather:

METAR KLGU 222151Z AUTO 20011G17KT 10SM CLR 32/03 A2994 RMK AO2 SLP083 T03170033

METAR KLGU 222251Z AUTO 19007KT 10SM CLR 32/02 A2993 RMK AO2 SLP075 T03170022