- Location: Gonzales, Texas
- Accident Number: CEN24LA141
- Date & Time: March 25, 2024, 18:53 Local
- Registration: N20MN
- Aircraft: Cozy Mark IV
- Aircraft Damage: Substantial
- Defining Event: Loss of engine power (total)
- Injuries: 1 None
- Flight Conducted Under: Part 91: General aviation - Personal
https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/193992/pdf
https://data.ntsb.gov/Docket?ProjectID=193992
On March 25, 2024, about 1853 central daylight time, a Cozy Mark IV airplane, N20MN, was substantially damaged when it was involved in an accident near Gonzales, Texas. The pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.
While enroute, at 9,500 ft above mean sea level (msl), the engine lost all power. After multiple attempts to restart the engine, the pilot executed a forced landing to a nearby airport. The airplane landed short of the runway threshold and its nose landing gear separated as the airplane transitioned onto the asphalt runway. The left wing and left canard sustained substantial damage.
Postaccident examination of the engine revealed that the left crankshaft idler gear shaft separated from its attach points, which prevented the crankshaft idler gear from engaging its corresponding crankshaft and camshaft gears. The disengagement prevented camshaft rotation and valvetrain timing to the crankshaft. The left crankshaft idler gear’s attachment hardware were both separated into two sections from abrasion. The capscrew was lockwired to the idler shaft but no lockwire was observed through the stud and slotted shear nut.
It is likely that maintenance personnel did not follow the engine manufacturer’s service instructions and undertorqued the fasteners during installation, resulting in insufficient clamping force. Additionally, the absence of lockwire likely permitted the shear nut to back off during engine operation. Because the airplane’s maintenance records were not available for review, the investigation was not able to identify when the crankshaft idler gear was last serviced.
- Probable Cause: Maintenance personnel’s failure to properly torque the crankshaft idler gear hardware according to the engine manufacturer’s service instructions, which resulted in separation of the crankshaft idler gear’s fasteners and disengagement of the camshaft, crankshaft, and crankshaft idler gear and a subsequent total loss of engine power.




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