Friday, April 03, 2026

Loss of control on ground: Piper PA-18-150 Super Cub, N3994Z, accident occurred on June 3, 2025, at Willow Airport (UUO/PAUO), Willow, Alaska

  • Location: Willow, Alaska 
  • Accident Number: ANC25LA071 
  • Date & Time: June 3, 2025, 09:30 Local 
  • Registration: N3994Z 
  • Aircraft: Piper PA-18-150 
  • Aircraft Damage: Substantial 
  • Defining Event: Loss of control on ground 
  • Injuries: 2 None 
  • Flight Conducted Under: Part 91: General aviation - Instructional

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/200508/pdf

https://data.ntsb.gov/Docket?ProjectID=200508

The flight instructor, seated in the rear seat, stated that he and the pilot receiving instruction, seated in the front seat, were practicing landings in a tailwheel-equipped airplane. The purpose of the flight was for the pilot that was receiving instruction to obtain a tailwheel endorsement.

During the landing rollout, gusting wind conditions lifted the left wing and the pilot receiving instruction applied right rudder, but the airplane continued to the right. The flight instructor then applied more right rudder; however, the airplane ground looped and sustained substantial damage to the right wing.

The instructor pilot reported that there were no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operation.

At the time of the accident, the pilot was landing on runway 13 with wind from 080° at 9 knots, gusting to 16 knots.

- Probable Cause: The flight instructor’s delayed remedial action/lack of supervision. Contributing to the accident was the pilot receiving instructions failure to maintain directional control during the landing roll in gusting wind conditions, which resulted in a ground loop.

Loss of control on ground: Temco GC-1B Swift, N78316, accident occurred on September 18, 2025, at South Lewis County Airport (TDO/KTDO), Toledo, Washington

  • Location: Toledo, Washington 
  • Accident Number: WPR25LA306 
  • Date & Time: September 18, 2025, 12:56 Local 
  • Registration: N78316 
  • Aircraft: Temco GC-1B 
  • Aircraft Damage: Substantial 
  • Defining Event: Loss of control on ground 
  • Injuries: 1 None 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/201817/pdf

https://data.ntsb.gov/Docket?ProjectID=201817

The pilot reported that as he prepared for takeoff in the tailwheel equipped airplane, he did not observe any movement of grass or trees due to wind. During the takeoff roll, the right wing rose suddenly, which the pilot counteracted with aileron inputs. The airplane bounced, and the right wing rose a second time, which the pilot counteracted. Subsequently, the airplane banked steeply to the left, exited the runway, and impacted the ground. The airplane sustained substantial damage to the fuselage, right aileron, and the elevator.

Prior to taxiing to and departing runway 24, the pilot observed a windsock, which indicated the wind was from about 260° at 2 to 6 knots. The airport manager reported there was a 20 knot crosswind at the time of the accident.

The pilot reported that there were no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation.

- Probable Cause: The pilot’s failure to maintain control of the airplane during takeoff in crosswind conditions.

Loss of control on ground: Maule M-7-235B Super Rocket, N116G, accident occurred on January 17, 2026, at Yellowstone Regional Airport (COD/KCOD), Cody, Wyoming

  • Location: Cody, Wyoming 
  • Accident Number: WPR26LA084 
  • Date & Time: January 17, 2026, 09:39 Local 
  • Registration: N116G 
  • Aircraft: Maule M-7-235B 
  • Aircraft Damage: Substantial 
  • Defining Event: Loss of control on ground 
  • Injuries: 5 None 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202316/pdf

https://data.ntsb.gov/Docket?ProjectID=202316

The pilot reported that during landing roll, the airplane began to move to the left, which he applied corrective control inputs to maneuver the airplane to the right. The pilot stated that as the airplane began to move to the right, it began to feel as if it was going to swing around. Subsequently, the left wing tip stuck the runway surface and the airplane swung about 270°, before it settled onto the right main landing gear, which collapsed. The airplane sustained substantial damage to the left wing, and both ailerons. At the time of the accident, the pilot was landing on runway 22 with calm wind.

The pilot reported no pre-accident mechanical failures or malfunctions with the airplane that would have precluded normal operation. 

- Probable Cause: The pilot's failure to maintain directional control during landing roll.

Landing area overshoot: Kitfox Series 7 Super Sport, N775DZ, accident occurred on January 19, 2026, near Lemmon Valley-Golden Valley, Nevada

  • Location: Lemmon Valley-Golden Valley, Nevada 
  • Accident Number: WPR26LA087 
  • Date & Time: January 19, 2026, 09:33 Local 
  • Registration: N775DZ 
  • Aircraft: Kitfox Series 7 
  • Aircraft Damage: Substantial 
  • Defining Event: Landing area overshoot 
  • Injuries: 1 Serious 
  • Flight Conducted Under: Part 91: General aviation - Personal 

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202327/pdf

https://data.ntsb.gov/Docket?ProjectID=202327

The pilot reported that he had performed a stop-and-go in a dirt clearing with a slight upslope. The pilot attempted to land in the clearing a second time, but during the landing flare, the pilot realized that he was going to land about 50 to 100 ft past his previous landing point and observed large sticks and a dirt mound in the available landing area ahead of the airplane. The pilot said that he initiated a go-around by applying full power and noted that he did not have the performance while in the low energy state. Subsequently, the landing gear briefly contacted the ground and the left wing dropped before the airplane impacted terrain. During the accident sequence, the left wing, left flaperon, and fuselage sustained substantial damage.

The pilot reported that there were no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation.

- Probable Cause: The pilot’s inability to maintain clearance from terrain during a go-around.

Thursday, April 02, 2026

Freedom Master FM-2 Air-Shark I, N220AS, fatal accident occurred on March 25, 2026, in Statesboro, Georiga

  • Location: Statesboro, GA 
  • Accident Number: CEN26FA147 
  • Date & Time: March 25, 2026, 14:53 Local 
  • Registration: N220AS 
  • Aircraft: Experimental Homebuilt Airshark 
  • Injuries: 1 Fatal 
  • Flight Conducted Under: Part 91: General aviation - Personal 

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202696/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N220AS

On March 25, 2026, about 1453 eastern daylight time, an experimental homebuilt Airshark airplane, N220AS, was substantially damaged when it was involved in an accident near Statesboro, Georgia. The pilot was fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91personal flight.

The airplane was being prepared for a ferry flight from Statesboro, Georgia, to Carrollton, Georgia, when one of the pilots decided to conduct a local flight to verify the airplane was performing normally before beginning the cross-country flight. Local authorities received a cell phone crash alert at 1453. First responders located the wreckage in a wheat field where it came to rest inverted.

The airplane struck a tree in about a 14° right wing low attitude about 42 feet above the ground on a 062° magnetic heading. A ground scar at 215 feet forward from the tree appeared to have been created by a propeller strike. At 218 feet from the tree, a large ground scar led up to the airplane which came to rest inverted 245 feet from the tree. An impression in the soil to the left of the large groundscar was consistent with the right wing as evidenced by the green position light lens found at the outer end of the impression.

An on site examination of the wreckage revealed no anomalies were found with the flight control system or flight control surfaces. Flight control continuity was verified for the ailerons, rudder, and elevators.

The airplane was reported to have been fueled to capacity (118 gallons) before the accident flight. The fuel selector in the cockpit was in the left fuel tank position. Both fuel tanks were breached, and the surrounding vegetation was yellow in the field where the wreckage came to rest. The right fuel cap and its receptacle were separated from the wing but present in the debris field next to the airplane. Both fuel caps were present and secure in their receptacles.

To facilitate viewing the fuel tank finger screens with a borescope, access holes were made in the wings near the wing root in the top wing skin. The right fuel tank finger screen was free of obstructions. The left fuel tank finger screen was corroded and appeared to be 30 to 40% obstructed. The obstruction’s appearance was consistent with solder used to manufacture the finger screen’s seam and end cap and did not appear to be foreign object debris from the fuel tank. Both fuel tanks were clean and free of debris in the area around the finger screens.

The airplane was equipped with a bail type gascolator and an inline paper element style fuel filter. The bail type gascolator bowl was sampled and blue liquid with an odor consistent with 100LL aviation fuel was collected in a container. When water-indicating paste was applied to the fuel, there was a small amount of water present (a tiny portion of the paste turned bright red). The gascolator bowl was removed and there was about a ½ teaspoon of water present. There was no filtering element or screen present in the gascolator bowl, and rust was present in the bottom of the bowl.

The paper style fuel filter was removed from its mount. It contained blue liquid consistent with the appearance and odor of 100LL aviation fuel. Water-indicating paste was added to the fuel. It did not indicate any water was present. The paper filter element was generally clean. Some rust and corrosion were present in the metal housing.

No leaks or anomalies were noted along the fuel lines in the airframe. Fuel was present in the engine compartment fuel lines and all the engine fuel system components examined. The fuel injector servo and fuel flow divider were disassembled and no anomalies were noted. The engine driven fuel pump was removed from the engine and produced air at the outlet port when it was actuated by hand. The unit was disassembled and no anomalies were noted.

The engine valve covers were removed and crankshaft continuity to the rear gears and to the valvetrain was confirmed. Compression and suction were observed from all six cylinders. A wire screen covered the fuel injector servo; corrosion and some trapped debris were present. No other induction air filtration system was present for this installation. Both magnetos exhibited impact damage. The left magneto did not produce spark when rotated by hand. The right magneto produced spark when it was rotated with a drill. The spark plug electrodes exhibited dark grey coloration and normal wear signatures. The No. 3 bottom spark plug electrodes were oil soaked. The ignition harness was secure and no damage was noted. Oil was observed in the engine. The oil suction screen contained about ¼ teaspoon of dark granular material. The oil filter was not examined due to impact damage.

The propeller remained attached to the engine. One blade was bent aft about 20° about 10 inches from its tip. One blade was curved aft about 50° about 12 inches from its tip. One blade was curved aft about 80° about 12 inches from its tip. All three blades were twisted in varying amounts towards their respective blade faces.

A Levil Flight Aviation broadcasting outer module (BOM) was found on the ground next to the airplane, which had been attached to one of the wing’s lower wing skin access covers. The unit is capable of providing flight data wirelessly to a phone or tablet in the cockpit when properly configured. The unit was reported to have been installed the day of the accident flight, but the contracted ferry flight pilot declined to configure the device due to time constraints. According to the manufacturer’s website, the unit may contain a flash memory card. The unit was retained for further examination.

Piper PA-28-140 Cherokee, N9913W, fatal accident occurred on March 20, 2026, near Whiteside County Airport (SQI/KSQI), Sterling, Illinois

  • Location: Rock Falls, IL 
  • Accident Number: CEN26FA141 
  • Date & Time: March 20, 2026, 15:03 Local 
  • Registration: N9913W 
  • Aircraft: Piper PA-28-140 
  • Injuries: 1 Fatal 
  • Flight Conducted Under: Part 91: General aviation - Instructional 

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202671/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N9913W

On March 20, 2026, about 1503 central daylight time, a Piper PA-28-140 airplane, N9913W, was destroyed when it was involved in an accident near Rock Falls, Illinois. The student pilot sustained fatal injuries. The airplane was being operated as a Title 14 Code of Federal Regulations Part 91 instructional flight.

The student pilot’s flight instructor stated that the student pilot arrived at the Whiteside County Airport (SQI) in Rock Falls, Illinois, around 1430 to complete his 10th solo flight since receiving his solo endorsement on February 12, 2026. According to the instructor the wind had been variable throughout the day and favored both runway 36 and runway 25 with windy conditions. The instructor stated that the student pilot was going to use runway 25 but was unsure what flight maneuver he was going perform for the local area flight.

At 1503, an automatic crash detection alert was received by local emergency services from the student pilot’s Apple iPhone. At 1510, first responders discovered the airplane upright in an agricultural field 1,100 ft south of runway 25. There were no witnesses who observed the accident.

The airplane came to rest upright on a heading of about 323°. The main debris field was about 36 ft in length on a heading of about 087° with the initial impact point ground scar containing fragments of the left wing tip and leading edge. A second impact ground depression was about 22 ft past the intimal impact point and contained forward fuselage debris. The left wing was separated from the airframe and found 67 ft past the initial impact point (see figure 1).


A secondary debris field extended past the airframe on a heading of about 087° and contained various baggage compartment items, sections of the cockpit instrument panel and interior, and personal items.

The right flap and flap control system were found in the full down position with the flap handle (Johnson bar) locked in that position. The flap handle was manipulated by hand and operated normally, however, the flap control cable between the bar and roller chain was jammed by impact damage and was unable to rotate the flap torque tube. Flight control continuity was established between all flight control surfaces and their respective cockpit controls. The elevator and aileron flight control cables had separations at the forward fuselage and spar box consistent with overload failure. The left pilot seat lap belt was found with the latch engaged but the left sidewall belt attachment pulled free from the airframe structure.

The engine crankshaft was rotated by hand by the propeller and continuity to the accessory section was established. The magnetos were removed and rotated with a drill with spark was observed on all leads. The engine driven fuel pump was also removed with fuel observed in the pump. The entire fuel system was found compromised and open to atmosphere in numerous locations consistent with impact damage. Fuel was only observed in the left fuel tank fuselage fuel line and the left wing fuel tank exhibited hydrologic deformation. No blockages were observed in the fuel lines, all fuel screens were clean, and the fuel selector operated normally.

The airplane was not equipped with an ADS-B Out transponder, and the Mode C transponder was found in the off position. The flight instructor stated that this was not unusual because the student pilot kept the radios off due to the airplane not being equipped with an avionics master switch.

A review of the student pilot’s logbook showed about 20 hours of recorded total flight time; 11.1 hours of dual instruction, and 3.8 hours of recorded solo time as of the logbook’s last entry on February 15, 2026. The flight instructor stated that the student pilot had flown an additional six solo and three dual instruction flights since February 15, 2026. Additionally, the student pilot had performed three unassisted takeoffs and landings with the flight instructor earlier in the day and the flight instructor had no concerns with him performing further solo flights.

A uAvionix Sentry ADS-B IN unit and an Apple iPhone were recovered and retained for further examination. 

Cessna 150G, N6305S, accident occurred on March 21, 2026, near Colorado Springs East Airport (CO4), Ellicott, Colorado

  • Location: Ellicott, CO 
  • Accident Number: CEN26LA156 
  • Date & Time: March 21, 2026, 10:23 Local 
  • Registration: N6305S 
  • Aircraft: Cessna 150G 
  • Injuries: 1 Serious 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202732/pdf

https://registry.faa.gov/aircraftinquiry/Search/NNumberResult?NNumberTxt=N6305S

On March 21, 2026, about 1023 mountain daylight time, a Cessna 150G airplane, N6305S, was substantially damaged when it was involved in an accident near Ellicott, Colorado. The pilot sustained serious injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported that he recalled completing a preflight inspection, a before takeoff engine run-up, and taxing onto the runway for takeoff. He did not recall any portion of the accident sequence.

A witness stated that the pilot intended to conduct some takeoffs and landings for currency. The pilot departed toward the south, and the takeoff appeared normal. The airplane went out of sight behind a hangar. However, when he regained sight of it, the airplane was on an easterly heading and in an approximate 60° left bank.

The airplane subsequently impacted the ground near wings level. It came to rest on a northeast heading about 100 ft before the departure end of the runway and about 500 ft left of the centerline. The airplane sustained damage to the fuselage, empennage, and both wings.  

Airframe and engine examinations are planned.

Piper PA-28-140 Cherokee, N7328J, accident occurred on March 21, 2026, near West Valley City, Utah

  • Location: West Valley City, UT 
  • Accident Number: WPR26LA132 
  • Date & Time: March 21, 2026, 16:10 Local 
  • Registration: N7328J 
  • Aircraft: Piper PA-28-140 
  • Injuries: 2 None 
  • Flight Conducted Under: Part 91: General aviation - Personal 

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202682/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N7328J

On March 21, 2026, about 1610 mountain daylight time, a Piper PA-28-140, N7328J, was substantially damaged when it was involved in an accident near West Valley City, Utah. The pilot and passenger were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported that they departed from the South Valley Regional Airport, Salt Lake City, Utah (SVR) for a local flight. While returning to the departure airport, at an altitude of about 5,800 ft mean sea level (msl), the engine experienced a partial loss of power. He utilized the airplane checklist to troubleshoot the loss of engine power, however, was unable to restore engine power. Unable to maintain altitude, he elected to make an off-airport landing on an open dirt field. During the landing roll, the airplane encountered rough terrain, the nose and right landing gear collapsed, and the airplane’s right wing impacted the dirt surface.

Postaccident examination of the airplane revealed that the right wing and aileron were substantially damaged. The wreckage was recovered for further examination.

Piper PA-28-140 Cherokee, N1653J, accident occurred on March 26, 2026, at Hall-Miller Municipal Airport (ATA/KATA), Atlanta, Texas

  • Location: Atlanta, TX 
  • Accident Number: CEN26LA149 
  • Date & Time: March 26, 2026, 07:20 Local 
  • Registration: N1653J 
  • Aircraft: Piper PA28 
  • Injuries: 1 None 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202701/pdf

https://registry.faa.gov/aircraftinquiry/Search/NNumberResult?NNumberTxt=1653J

On March 26, 2026, about 0720 central daylight time, a Piper PA28-140 airplane, N1653J, was substantially damaged when it was involved in an accident near Atlanta, Texas. The pilot was not injured. The flight was operated under the provisions of Title 14 Code of Federal Regulations Part 91 as a personal flight.

According to preliminary information obtained from the pilot, during the initial climb and while still over the runway, the airplane experienced a total loss of engine power. The pilot elected to land straight ahead, touching down just past the runway in a grassy area. During the landing rollout, the airplane collided with the airport’s perimeter chain link fence resulting in substantial damage to the fuselage.

A FAA inspector responded to the accident site and found fuel in both wing tanks. Sumped fuel from the tanks showed no evidence of water contamination. The airplane had recently been fueled, and the airport’s fuel also showed no evidence of contamination.

The airplane was retained for further examination.

Cessna 172G Skyhawk, N345QA, accident occurred on September 13, 2025, at Williston Municipal Airport (X60), Williston, Florida

  • Location: Williston, FL 
  • Accident Number: ERA25LA345 
  • Date & Time: September 13, 2025, 07:33 Local 
  • Registration: N345QA 
  • Aircraft: Cessna 172 
  • Injuries: 1 None 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/201000/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N345QA

On September 13, 2025, about 0733 eastern daylight time, a Cessna 172G, N345QA, was substantially damaged when it was involved in an accident near Williston, Florida. The pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported that the flight departed Orlando Executive Airport (ORL), Orlando, Florida, about 0600 with 17 gallons of fuel onboard, overflew Cross City Airport (CTY), Cross City, Florida, and was scheduled to land at Williston Regional Airport (X60), Williston, Florida.

About 1.5 hours after departure, while the airplane transitioned from the base leg to the final leg of the airport traffic pattern for runway 05 at X60, the engine experienced a momentary loss of power, followed shortly thereafter by a total loss of power. The pilot was unable to restore power to the engine and performed a forced landing to a field. During the landing roll, the nose landing gear collapsed, the airplane nosed over and came to rest in a grass field about 0.25-mile from the approach end of runway 05. The airplane sustained substantial damage to the fuselage and left wing strut.

The airplane was retained for further examination. 

Piper PA-30-160 Twin Comanche B, N811LE, accident occurred on February 23, 2026, at Big Bear Airport (L35), Big Bear City, California

  • Location: Big Bear, CA 
  • Accident Number: WPR26LA107 
  • Date & Time: February 23, 2026, 18:00 Local 
  • Registration: N811LE 
  • Aircraft: Piper PA-30 
  • Injuries: 2 None 
  • Flight Conducted Under: Part 91: General aviation - Personal 

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202498/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N811LE

On February 23, 2026, at 1800 Pacific standard time, a Piper PA-30, N811LE, was substantially damaged when it was involved in an accident near Big Bear, California. The pilot and passenger were not injured. The airplane was operated as a 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported an uneventful flight from Montgomery-Gibbs Executive Airport (MYF), San Diego, California, to Big Bear City Airport (L35), Big Bear, California. Upon arrival at L35, the pilot extended the landing gear and saw that the nose landing gear was extended down, but the green landing gear light was not illuminated. After touchdown, the landing gear collapsed, and the airplane slid down the runway, which resulted in damage to the fuselage undercarriage.

The airplane was recovered to a secure facility for further examination.

Cessna 177B Cardinal, N12984, accident occurred on February 21, 2026, near Rocky Junction, Arizona

  • Location: Rocky Junction, AZ 
  • Accident Number: ANC26LA016 
  • Date & Time: February 21, 2026, 17:46 Local 
  • Registration: N12984 
  • Aircraft: Cessna 177B 
  • Injuries: 2 Minor 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202488/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N12984

On February 21, 2026, 1746 Mountain standard time, a Cessna 177B airplane, N12984, was substantially damaged when it was involved in an accident near Rocky Junction, Arizona. The pilot and passenger sustain minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91personal flight.

The pilot reported that during departure at about 6,500ft msl (means sea level) the engine loss total power. The pilot observed one of the cylinder head temperatures was over 460 degrees. The pilot turned on the fuel boost pumps, changed fuel tanks but was unable to restart the engine. The pilot made a forced landing into remote hilly terrain. The airplane sustained substantial damage to the fuselage and both wings.

A postaccident examination of the wreckage is pending the recovery of the aircraft.

Bell 505 Jet Ranger X, N911FW, accident occurred on March 7, 2026, near Fort Worth Meacham International Airport (FTW/KFTW), Fort Worth, Texas

  • Location: Fort Worth, TX 
  • Accident Number: ANC26LA018 
  • Date & Time: March 7, 2026, 22:10 Local 
  • Registration: N911FW 
  • Aircraft: BELL TEXTRON CANADA LTD 505 
  • Injuries: 2 None 
  • Flight Conducted Under: Public aircraft 

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202617/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N911FW

On March 7, 2026, at 2210 Central daylight time, a Bell Textron 505 helicopter, N911FW, was substantially damaged when it was involved in an accident near Fort Worth, Texas. The pilot and crew member were not injured. The helicopter was operated as a Title 14 Code of Federal Regulations Part 91 public use flight.

The pilot reported that during takeoff, as the helicopter was climbing above the trees the engine power decreased to idle power. The pilot performed a forced landing to an open grass field. The helicopter sustained substantial damage to the vertical stabilizer.

A post examination of the wreckage is pending.

Wednesday, April 01, 2026

Robinson R44 Raven I, N478AT, fatal accident occurred on March 23, 2026, in Boynton Beach, Florida

  • Location: Boynton Beach, FL 
  • Accident Number: ANC26FA021 
  • Date & Time: March 23, 2026, 12:21 Local 
  • Registration: N478AT 
  • Aircraft: ROBINSON HELICOPTER R44 
  • Injuries: 2 Fatal 
  • Flight Conducted Under: Part 91: General aviation - Instructional 

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/202678/pdf

https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=478AT

On March 23, 2026, about 1221 eastern daylight time, a Robinson R44 Raven I helicopter, N478AT, was destroyed when it was involved in an accident near Boynton Beach, Florida. The flight instructor and the pilot receiving instruction were fatally injured. The helicopter was operated as a Title 14 Code of Federal Regulations Part 91 instructional flight.

According to the flight school, Palm Beach Helicopters, the flight instructor, who was seated in the left seat, and the pilot receiving instruction, who was seated in the right seat, departed the Palm Beach County Park Airport (LNA), Latana, Florida, at 1124. The purpose of the flight was to provide the pilot receiving instruction with a basic visual flight rules (VFR) orientation flight, which was to include going to the Downtown Fort Lauderdale Heliport (DT1) in Fort Lauderdale, Florida, and then returning to LNA. Records indicated that 23 gallons of fuel was added to the helicopter just before departure and that the total amount of fuel onboard was 46.5 gallons.

The helicopter was equipped with ADS-B, which provided helicopter position information, as well as SPOT Trace, which enabled both flight tracking and two-way text communication. According to the ADS-B data, the helicopter departed LNA and flew south along the coastline and conducted a landing at DT1.

After departing DT1, the helicopter flew northwest, then made a turn back to the east. A review of archived voice communication information from the LNA common traffic advisory frequency (CTAF) revealed that the flight instructor first reported their position to be “7 [miles] to the south, straight in for [runway] 34.” About 27 seconds later, the flight instructor made another radio call and reported to a company helicopter that “we’re going to be landing out here in one of these fields, we’ve got something going on with the helicopter.” About 12 seconds later, the company helicopter attempted to contact N478AT, but they did not respond.

Witnesses reported seeing the helicopter flying low before it suddenly entered a steep right turn with a nose-low attitude. Subsequently, the helicopter impacted the roof of a vacant warehouse about 6 miles south of LNA and came to rest inverted inside the building. During the impact sequence, the helicopter severed a water line for the building’s sprinkler system, dispersing a large amount of water on the wreckage. There was no postaccident fire.

The main rotor and main rotor gear box were found suspended within the warehouse roof structure, and the main wreckage came to rest inverted below it. The engine core was found in the main wreckage behind the cockpit with the forward engine mounts separated and the aft mount still secured to the airframe. The tailboom was found secured to the airframe, and the tailrotor and empennage were found impact separated and within the main wreckage (see figure 1). 

During the NTSB’s on-site examination of the main rotor flight controls, the upper right pushpull tube was found separated from the lower rod end (part number D173-2), which remained attached to the upper hydraulic servo piston shaft at the clevis (part number D200-1). The palnut and jam nut that secure the upper right push-pull tube to the rod end could not be rotated by hand on the rod end threads. The upper right push-pull tube was observed to be elongated at the threaded end (see figure 2). Remnants of torque stripe paint was present on the push-pull tube, palnut, and jam nut.


The palnuts and jam nuts on the left and aft lower rod ends (part number D173-2) and below the hydraulic servo clevis were found to be finger tight. Varying degrees of corrosion was observed on the palnuts and jam nuts.

Examination of the engine did not reveal any mechanical anomaly or malfunction that would have precluded normal operation.

A review of the airframe maintenance records showed that the most recent maintenance was a 100-hour inspection, which was completed on March 23, 2026, at an airframe total time of 7,486.6 hours and a tach time of 3,091.1 hours. The most recent annual inspection was completed on June 18, 2025, at an airframe total time of 7,090 hours and a tach time of 2,694.7 hours. At the time of the accident, the tach time was 3,092.08 hours, and the engine total time since overhaul was 894 hours.

The flight instructor held flight instructor and commercial pilot certificates with a rating for rotorcraft helicopters, a ground instructor certificate, and a remote pilot certificate. He held a first-class medical certificate issued April 2, 2025, without limitations. According to pilot records obtained from the flight school, the flight instructor had about 822 total hours of civilian flight experience and about 140 hours in the accident helicopter make and model.

The pilot receiving instruction held an airline transport pilot certificate with a rating for airplane single-engine land and a commercial pilot certificate with ratings for airplane single-engine land, rotorcraft helicopter, and instrument helicopter. He held a first-class medical certificate issued February 28, 2026, with the limitation, “Not valid for any class after [February 28, 2027]. Must use corrective lens(es) to meet vision standards at all required distances.” On his application for the medical certificate, the pilot reported 5,725 total hours of civilian flight experience and 225 hours in the preceding 6 months.

The three hydraulic servos, push-pull tubes, and rod ends were transported to the NTSB Materials Laboratory, Washington, D.C., for additional examination. 

Loss of control in flight: Airmax SeaMax M-22, N154RL, accident occurred on May 17, 2025, near Dahlgren Center, Virginia

  • Location: Dahlgren Center, Virginia 
  • Accident Number: ERA25LA203 
  • Date & Time: May 17, 2025, 16:00 Local 
  • Registration: N154RL 
  • Aircraft: SEAMAX AIRCRAFT LTDA SEAMAX M-22 
  • Aircraft Damage: Substantial 
  • Defining Event: Loss of control in flight 
  • Injuries: 1 Serious 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/200177/pdf

https://data.ntsb.gov/Docket?ProjectID=200177

On May 17, 2025, about 1600 eastern daylight time, a special light sport amphibious Seamax M-22 airplane, N154RL, was substantially damaged when it was involved in an accident near Dahlgren, Virginia. The pilot sustained serious injuries. The airplane was being operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

After three aborted upwind water takeoff attempts due to water washing over the cockpit area and obstructing the view, the pilot attempted a downwind takeoff that prevented the water from cresting over the cockpit. Video footage showed that, after what appeared to be a normal takeoff run, the airplane rotated and lifted off; however, during the initial climb the airplane appeared to struggle to ascend. The wings rocked back and forth as the airplane climbed to about 200 ft above the water surface. The pilot then made a left turn; shortly after, the left wing dropped, and the airplane abruptly descended in a left spiral until it impacted the water.

On-board engine parameter data showed normal engine operation until the moment of impact. Postaccident airframe and engine examination did not reveal any preimpact malfunction or anomaly that would preclude normal operation or performance. While taking off with a tailwind and during the subsequent climb, the pilot likely failed to maintain adequate airspeed during the turn, which resulted in the exceedance of the airplane’s critical angle of attack and an aerodynamic stall. The airplane’s low altitude prevented recovery.

- Probable Cause: The pilot’s failure to maintain adequate airspeed and his exceedance of the airplane’s critical angle of attack during the initial climb, which resulted in an aerodynamic stall. Contributing to the accident was the pilot’s decision to take off with a known tailwind.

Fire/smoke (non-impact): Beechcraft V35B Bonanza, N6659L, fatal accident occurred on February 1, 2024, in Clearwater, Florida

  • Location: Clearwater, Florida 
  • Accident Number: ERA24FA104 
  • Date & Time: February 1, 2024, 19:07 Local 
  • Registration: N6659L Aircraft: Beech V35 
  • Aircraft Damage: Destroyed 
  • Defining Event: Fire/smoke (non-impact) 
  • Injuries: 3 Fatal, 1 Minor 
  • Flight Conducted Under: Part 91: General aviation - Personal

https://data.ntsb.gov/carol-repgen/api/Aviation/ReportMain/GenerateNewestReport/193737/pdf

https://data.ntsb.gov/Docket?ProjectID=193737

On February 1, 2024, about 1907 eastern standard time, a Beech V35B airplane, N6659L, was destroyed when it impacted two residences and the ground near Clearwater, Florida. The commercial pilot and two occupants of one residence were fatally injured, and one occupant of the other residence sustained minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot proceeded toward the destination airport, cancelled his instrument flight rules (IFR) clearance when about 5 nautical miles (nm) from the airport, then proceeded under visual flight rules (VFR) in night visual weather conditions. The airport, with which the pilot was unfamiliar, was non-towered, located in a densely populated area, and not equipped with a rotating beacon. After establishing contact on the airport’s common traffic advisory frequency (CTAF), the pilot announced that he was unable to locate the airport and asked repeatedly for the pilot-controlled runway lights to be turned on.

According to witnesses who were in the airport’s fixed based operator (FBO) facility and heard the CTAF communications, at the time of the pilot’s first request, the runway lights were already on medium intensity from an airplane that had just landed. One of the witnesses responded to the pilot’s request by keying the radio microphone seven times to turn the lights up to high intensity. The witnesses and pilots in a nearby airplane reported that they subsequently heard the pilot announce that he had a fire. One witness at the FBO asked the pilot to repeat what he said, but the pilot did not.

ADS-B data showed that the flight had approached the airport from the southeast headed northwest. Once it reached the airport, it proceeded northwest, parallel to and about 0.5 nm west of the runway, before continuing northwest and past the airport. It subsequently turned left (to the west, away from the airport), completed a 180° turn, then again passed the airport before continuing south.

About 2 minutes before the accident, the flight was flying about 900 ft pressure altitude, and the pilot set the transponder to emergency code 7700. The flight proceeded briefly east, then southeast. About 1 minute before the accident, the pilot reestablished contact with the air traffic controller at the facility with which he had previously canceled his IFR clearance. The pilot told the controller that he was proceeding to a different airport because he was unable to visually identify his original destination airport.

The controller advised the pilot that the flight was 1 mile south of his original destination airport then asked the pilot if he could turn to a heading 180° and maintain the present altitude. The pilot advised the controller, “I’m losing engine.” According to a sound spectrum study, at the time of this communication, the airplane’s engine was operating at 2,500 rpm. The controller asked the pilot if he could see another airport that was 3 miles ahead of his position (and closer than the alternative airport that the pilot mentioned), but the pilot did not respond. The flight continued southeast, then turned left and descended steeply until impact.

According to a review of the available data, during the airplane’s final 20-second descent, it attained a maximum descent rate of 5,836 ft per minute (fpm) and the groundspeed increased. Per the sound spectrum study, the engine rpm decreased to about 2,053 then was estimated to about 1,907 immediately before impact. Witnesses on the ground who saw the airplane’s descent reported seeing fire on the forward portion of the airplane. Although the engine rpm decreased immediately before impact, it could not be determined what the pilot meant when he advised the controller that he was losing the engine because, at that time, it was operating at 2,500 rpm, which was slightly below the maximum continuous takeoff propeller rpm.

Postaccident examination of the flight controls and engine drivetrain, ignition, air induction, exhaust, and lubrication systems revealed no evidence of preimpact failure or malfunction. The outlet fitting of the metering valve was impact-fractured, and the b-nut of the flexible fuel hose attached to this outlet fitting was not fully tight. The throttle body and metering valve and corresponding area of the engine oil sump exhibited clean burn areas without soot deposits, though after coming to rest those areas were shielded by dirt and the upwardly crushed engine cowlings.

No discrepancy with the threads of the flexible fuel hose or of the fractured outlet fitting at the metering valve was identified, and it was possible to successfully torque the b-nut to about the minimum specified value. Further, several other fuel fittings in the engine compartment were also impact-fractured (similar to the fractured outlet fitting), but their respective hoses’ b-nuts remained tightly secured.

The engine was installed about 7.5 years before the accident, and there was no record of any maintenance done to the area of the loose b-nut since. The engine had accumulated 583 operating hours since installation, so it is unlikely that the hose was not tightly secured at that time. It is also unlikely that it was loosened by impact or the effects of the postcrash fire. It is more likely that, at some point after engine installation, undocumented maintenance occurred to the fuel hose from the metering valve to the manifold valve, and unknown maintenance personnel failed to adequately torque the fuel hose b-nut at the metering valve outlet fitting.

Based on the severity of the observed thermal damage in the area of the throttle body and metering valve, the most likely fire scenario for the accident airplane was an in-flight fire occurring due to ignition of fuel leaking from the slightly loose fuel hose at the outlet of the fuel metering valve.

The steep descent immediately before impact was the pilot’s likely response to the in-flight engine compartment fire and his initiation of an emergency descent. Though the position of the fuel selector valve was found between the left and right tank positions, and the position at impact could not be determined from the available evidence, the engine rpm about 43 seconds before impact was 2,500. Although the engine rpm had decreased immediately before impact, it is likely that the pilot did not promptly turn off the fuel selector in accordance with the “Engine Fire in Flight” checklist after recognizing and reporting a fire on the destination airport’s CTAF. Thus, had the pilot promptly secured the fuel selector valve and in conjunction with the steep descent, it is possible that the extent of the in-flight fire could have been mitigated. Further, had the pilot been able to visually locate the destination airport, it is likely that the he could have landed the airplane earlier in the accident sequence.

The pilot had negative results for carboxyhemoglobin, and no pre-existing issue was found at autopsy. Thus, it is unlikely that any medical issue resulted in the pilot’s failure to arrest the airplane’s steep rate of descent before impact with the residences.

- Probable Cause: An in-flight engine compartment fire due to a partially loose flexible fuel hose b-nut at the fuel metering unit. Contributing to the severity of the accident was the pilot’s inability to visually identify the destination airport at night, which prolonged the in-flight emergency.